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|
Attributes | |
ACN | 417485 |
Time | |
Date | 199810 |
Day | Mon |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : bgm airport : bgm |
State Reference | NY |
Altitude | agl bound lower : 0 agl bound upper : 50 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : bgm tower : slc |
Operator | common carrier : air carrier |
Make Model Name | Jetstream 32 |
Operating Under FAR Part | Part 121 |
Navigation In Use | Other Other |
Flight Phase | climbout : takeoff |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial pilot : cfi |
Experience | flight time last 90 days : 185 flight time total : 2710 flight time type : 1267 |
ASRS Report | 417485 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : cfi pilot : instrument pilot : commercial |
Experience | flight time last 90 days : 240 flight time total : 2800 flight time type : 1400 |
ASRS Report | 417487 |
Events | |
Anomaly | aircraft equipment problem : critical inflight encounter other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : declared emergency none taken : unable other |
Consequence | other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
A large seagull was ingested into #2 engine causing a flameout immediately following rotation. First officer flew standard single engine profile in right traffic visually. Captain/crew executed single engine memory procedures and found that #2 engine had relit and was providing some power. All engine indications were normal, but engine had a loud whining noise and aircraft handling suggested partial power loss from #2 engine. Captain declared emergency and notified ATC, company, and passenger. All relevant checklists were reviewed including single engine procedures (crew elected to keep partial power engine running). After uneventful flaps 20 degree landing and roll onto taxiway, #2 engine was shut down, but caught on fire. Crew proceeded with emergency evacuate/evacuation procedures. All 18 passenger and 2 crew deplaned without injuries. Good training and excellent crew resource management contributed to the successful outcome of this bird strike.
Original NASA ASRS Text
Title: BA32 FLC RETURN TO BGM AFTER LOSS OF ENG DUE TO BIRD STRIKE.
Narrative: A LARGE SEAGULL WAS INGESTED INTO #2 ENG CAUSING A FLAMEOUT IMMEDIATELY FOLLOWING ROTATION. FO FLEW STANDARD SINGLE ENG PROFILE IN R TFC VISUALLY. CAPT/CREW EXECUTED SINGLE ENG MEMORY PROCS AND FOUND THAT #2 ENG HAD RELIT AND WAS PROVIDING SOME PWR. ALL ENG INDICATIONS WERE NORMAL, BUT ENG HAD A LOUD WHINING NOISE AND ACFT HANDLING SUGGESTED PARTIAL PWR LOSS FROM #2 ENG. CAPT DECLARED EMER AND NOTIFIED ATC, COMPANY, AND PAX. ALL RELEVANT CHKLISTS WERE REVIEWED INCLUDING SINGLE ENG PROCS (CREW ELECTED TO KEEP PARTIAL PWR ENG RUNNING). AFTER UNEVENTFUL FLAPS 20 DEG LNDG AND ROLL ONTO TXWY, #2 ENG WAS SHUT DOWN, BUT CAUGHT ON FIRE. CREW PROCEEDED WITH EMER EVAC PROCS. ALL 18 PAX AND 2 CREW DEPLANED WITHOUT INJURIES. GOOD TRAINING AND EXCELLENT CREW RESOURCE MGMNT CONTRIBUTED TO THE SUCCESSFUL OUTCOME OF THIS BIRD STRIKE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.