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|
Attributes | |
ACN | 432331 |
Time | |
Date | 199903 |
Day | Sat |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : mia.airport |
State Reference | FL |
Altitude | agl single value : 1000 |
Environment | |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tracon : mia.tracon |
Operator | common carrier : air carrier |
Make Model Name | B727-200 |
Operating Under FAR Part | Part 121 |
Navigation In Use | other vortac |
Flight Phase | climbout : takeoff |
Route In Use | departure sid : mia 3 dept |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Qualification | flight attendant : currently qualified flight attendant aircraft qualified on : 5 |
Experience | flight attendant time airline total : 20 flight attendant time total : 20 flight attendant time type : 5 |
ASRS Report | 432331 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa other other : cab 1 |
Resolutory Action | controller : issued new clearance flight crew : landed as precaution |
Consequence | other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
Normal operation until takeoff. We heard a muffled sound -- like a pop. Shortly after that, captain reported a problem -- it was sensor or valve pressure (I don't recall) and said we would be landing back in mia in 10(?) mins. We were not asked to do a planned emergency, and landing was uneventful. We stayed with the passenger until the problem was fixed -- about 40 mins. No further incidence. We took the same plane to sju. Problem corrected by maintenance. Callback conversation with reporter revealed the following information: the reporter stated the aircraft was a B727-200 and had a full passenger load. The reporter said the cause of the return to the field was unknown as neither the flight crew nor maintenance shared this information with the cabin crew.
Original NASA ASRS Text
Title: A B727-200 ON TKOF EXPERIENCED A MECHANICAL PROB AND RETURNED TO THE FIELD.
Narrative: NORMAL OP UNTIL TKOF. WE HEARD A MUFFLED SOUND -- LIKE A POP. SHORTLY AFTER THAT, CAPT RPTED A PROB -- IT WAS SENSOR OR VALVE PRESSURE (I DON'T RECALL) AND SAID WE WOULD BE LNDG BACK IN MIA IN 10(?) MINS. WE WERE NOT ASKED TO DO A PLANNED EMER, AND LNDG WAS UNEVENTFUL. WE STAYED WITH THE PAX UNTIL THE PROB WAS FIXED -- ABOUT 40 MINS. NO FURTHER INCIDENCE. WE TOOK THE SAME PLANE TO SJU. PROB CORRECTED BY MAINT. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE ACFT WAS A B727-200 AND HAD A FULL PAX LOAD. THE RPTR SAID THE CAUSE OF THE RETURN TO THE FIELD WAS UNKNOWN AS NEITHER THE FLC NOR MAINT SHARED THIS INFO WITH THE CABIN CREW.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.