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|
Attributes | |
ACN | 432572 |
Time | |
Date | 199903 |
Day | Wed |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : san.airport |
State Reference | CA |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : san.tower tower : bos.tower |
Operator | common carrier : air carrier |
Make Model Name | Jetstream 32 |
Operating Under FAR Part | Part 135 |
Flight Phase | ground : takeoff roll |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 150 flight time total : 4600 flight time type : 2300 |
ASRS Report | 432572 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument pilot : multi engine |
Events | |
Anomaly | aircraft equipment problem : less severe other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : rpm indicator other flight crewa |
Resolutory Action | flight crew : rejected takeoff |
Consequence | faa : investigated |
Supplementary | |
Problem Areas | Flight Crew Human Performance Aircraft |
Primary Problem | Flight Crew Human Performance |
Narrative:
As we began to accelerate on the takeoff roll, I noticed a slight fluctuation with the left RPM gauge. Prior to 70 KTS, I elected to abort and taxied clear of the runway. I immediately determined that the left RPM lever had crept back slightly. I reset it to 100% and tightened the friction lock. The first officer and I agreed that this was the cause of the fluctuation. A subsequent full power runup confirmed this and nothing out of the ordinary was noted. 1 day after this, I have been informed that the FAA is inquiring about this. As I understand it, they would like to know why I did not return to the gate and/or write anything up. It was a simple case of the RPM lever creeping back slightly because the friction lock was not tight enough. There were not any mechanical malfunctions. We remedied the situation by tightening the friction lock.
Original NASA ASRS Text
Title: A JETSTREAM 3200 REJECTED TKOF DUE TO FLUCTUATING L ENG RPM CAUSED BY A LOOSE THROTTLE LOCK.
Narrative: AS WE BEGAN TO ACCELERATE ON THE TKOF ROLL, I NOTICED A SLIGHT FLUCTUATION WITH THE L RPM GAUGE. PRIOR TO 70 KTS, I ELECTED TO ABORT AND TAXIED CLR OF THE RWY. I IMMEDIATELY DETERMINED THAT THE L RPM LEVER HAD CREPT BACK SLIGHTLY. I RESET IT TO 100% AND TIGHTENED THE FRICTION LOCK. THE FO AND I AGREED THAT THIS WAS THE CAUSE OF THE FLUCTUATION. A SUBSEQUENT FULL PWR RUNUP CONFIRMED THIS AND NOTHING OUT OF THE ORDINARY WAS NOTED. 1 DAY AFTER THIS, I HAVE BEEN INFORMED THAT THE FAA IS INQUIRING ABOUT THIS. AS I UNDERSTAND IT, THEY WOULD LIKE TO KNOW WHY I DID NOT RETURN TO THE GATE AND/OR WRITE ANYTHING UP. IT WAS A SIMPLE CASE OF THE RPM LEVER CREEPING BACK SLIGHTLY BECAUSE THE FRICTION LOCK WAS NOT TIGHT ENOUGH. THERE WERE NOT ANY MECHANICAL MALFUNCTIONS. WE REMEDIED THE SIT BY TIGHTENING THE FRICTION LOCK.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.