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|
Attributes | |
ACN | 433910 |
Time | |
Date | 199904 |
Day | Tue |
Local Time Of Day | 0601 To 1200 |
Place | |
State Reference | ND |
Altitude | msl single value : 7000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zmp.artcc |
Operator | common carrier : air carrier |
Make Model Name | DC-9 40 |
Operating Under FAR Part | Part 121 |
Flight Phase | climbout : intermediate altitude |
Route In Use | departure : other published ifr departure enroute : on vectors |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : commercial pilot : flight engineer pilot : instrument pilot : multi engine pilot : private |
Experience | flight time last 90 days : 145 flight time total : 9044 flight time type : 260 |
ASRS Report | 433910 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument pilot : multi engine |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : far non adherence : published procedure other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : cabin altitude indicator other flight crewa other flight crewb |
Resolutory Action | controller : issued new clearance flight crew : overcame equipment problem none taken : anomaly accepted other |
Consequence | other |
Supplementary | |
Problem Areas | Flight Crew Human Performance Aircraft Company |
Primary Problem | Flight Crew Human Performance |
Narrative:
Aircraft did not pressurize after departure. Leveled off at 7000 ft and performed company operating manual procedures, which did not work. Had good air conditioning pressure from both packs and manually closed outflow valve. All door annunciator lights tested properly and indicated closed (lights out). Called company dispatch/maintenance control on radio for more assistance. Agreed to continue to msp since we had plenty of fuel, with new fuel consumption numbers. Just past 1/2 way to msp, lead flight attendant reported lots of wind noise in aft cabin and floor was cold in aft cabin. Landed in msp with no problems. Aft cargo door found fully open by maintenance control personnel upon arrival at gate. Annunciator lights still tested properly and indicated closed. Bad door sensor plug. MEL'ed item in msp. Did not lose any baggage according to ground service. Callback conversation with reporter revealed the following information: the reporter stated the condition the door was found on arrival at msp was cargo door fully open and the cargo net installed. The reporter said the door warning still tested ok on the ground at msp. The reporter said maintenance found a defective connector on the door sensor which was deferred as no parts were available at msp.
Original NASA ASRS Text
Title: A DC9-40 WAS DISPATCHED IN NON COMPLIANCE WITH THE AFT CARGO DOOR OPEN.
Narrative: ACFT DID NOT PRESSURIZE AFTER DEP. LEVELED OFF AT 7000 FT AND PERFORMED COMPANY OPERATING MANUAL PROCS, WHICH DID NOT WORK. HAD GOOD AIR CONDITIONING PRESSURE FROM BOTH PACKS AND MANUALLY CLOSED OUTFLOW VALVE. ALL DOOR ANNUNCIATOR LIGHTS TESTED PROPERLY AND INDICATED CLOSED (LIGHTS OUT). CALLED COMPANY DISPATCH/MAINT CTL ON RADIO FOR MORE ASSISTANCE. AGREED TO CONTINUE TO MSP SINCE WE HAD PLENTY OF FUEL, WITH NEW FUEL CONSUMPTION NUMBERS. JUST PAST 1/2 WAY TO MSP, LEAD FLT ATTENDANT RPTED LOTS OF WIND NOISE IN AFT CABIN AND FLOOR WAS COLD IN AFT CABIN. LANDED IN MSP WITH NO PROBS. AFT CARGO DOOR FOUND FULLY OPEN BY MAINT CTL PERSONNEL UPON ARR AT GATE. ANNUNCIATOR LIGHTS STILL TESTED PROPERLY AND INDICATED CLOSED. BAD DOOR SENSOR PLUG. MEL'ED ITEM IN MSP. DID NOT LOSE ANY BAGGAGE ACCORDING TO GND SVC. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED THE CONDITION THE DOOR WAS FOUND ON ARR AT MSP WAS CARGO DOOR FULLY OPEN AND THE CARGO NET INSTALLED. THE RPTR SAID THE DOOR WARNING STILL TESTED OK ON THE GND AT MSP. THE RPTR SAID MAINT FOUND A DEFECTIVE CONNECTOR ON THE DOOR SENSOR WHICH WAS DEFERRED AS NO PARTS WERE AVAILABLE AT MSP.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.