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|
Attributes | |
ACN | 437993 |
Time | |
Date | 199905 |
Day | Wed |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : atl.airport |
State Reference | GA |
Altitude | msl single value : 3500 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : ztl.artcc |
Operator | common carrier : air carrier |
Make Model Name | B727-200 |
Operating Under FAR Part | Part 121 |
Flight Phase | cruise : level |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : cfi pilot : flight engineer pilot : multi engine pilot : atp |
Experience | flight time last 90 days : 240 flight time total : 14800 flight time type : 10700 |
ASRS Report | 437993 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : multi engine pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : less severe inflight encounter other non adherence : far other anomaly other |
Consequence | other other |
Supplementary | |
Problem Areas | Flight Crew Human Performance Aircraft |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
Crew departed atl atl-dtw. Shortly after leveloff in cruise, so observed crew oxygen pressure indication of approximately 800 psi. Oxygen pressure was in normal range (above 1400 psi) on preflight in atl. There were 3 pilots and 1 cockpit jump seat rider. Crew determined that loss of crew oxygen pressure had been caused by oxygen flowing from first officer's oxygen mask. The 'emergency on' position on the oxygen mask control panel was found to have been inadvertently 'bumped' into the on position. The switch was immediately reselected to the normal position. Crew discussed potential for use of supplemental oxygen and descended to 17000 ft MSL. Captain consulted dispatch and maintenance control to evaluate additional considerations and to coordinate maintenance in dtw. Flight operated normally to dtw.
Original NASA ASRS Text
Title: B727 CREW DISCOVERS AT LEVELOFF THAT CREW OXYGEN SUPPLY HAS DECREASED TO 800 PSI.
Narrative: CREW DEPARTED ATL ATL-DTW. SHORTLY AFTER LEVELOFF IN CRUISE, SO OBSERVED CREW OXYGEN PRESSURE INDICATION OF APPROX 800 PSI. OXYGEN PRESSURE WAS IN NORMAL RANGE (ABOVE 1400 PSI) ON PREFLT IN ATL. THERE WERE 3 PLTS AND 1 COCKPIT JUMP SEAT RIDER. CREW DETERMINED THAT LOSS OF CREW OXYGEN PRESSURE HAD BEEN CAUSED BY OXYGEN FLOWING FROM FO'S OXYGEN MASK. THE 'EMER ON' POS ON THE OXYGEN MASK CTL PANEL WAS FOUND TO HAVE BEEN INADVERTENTLY 'BUMPED' INTO THE ON POS. THE SWITCH WAS IMMEDIATELY RESELECTED TO THE NORMAL POS. CREW DISCUSSED POTENTIAL FOR USE OF SUPPLEMENTAL OXYGEN AND DSNDED TO 17000 FT MSL. CAPT CONSULTED DISPATCH AND MAINT CTL TO EVALUATE ADDITIONAL CONSIDERATIONS AND TO COORDINATE MAINT IN DTW. FLT OPERATED NORMALLY TO DTW.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.