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|
Attributes | |
ACN | 449692 |
Time | |
Date | 199909 |
Day | Mon |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : bdr.airport |
State Reference | CT |
Altitude | msl bound lower : 10 msl bound upper : 1000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : bdr.tower |
Operator | general aviation : personal |
Make Model Name | Baron 55/Cochise |
Operating Under FAR Part | Part 91 |
Navigation In Use | other |
Flight Phase | climbout : intermediate altitude climbout : initial |
Flight Plan | None |
Person 1 | |
Affiliation | other |
Function | instruction : instructor |
Qualification | pilot : cfi pilot : instrument pilot : multi engine pilot : commercial |
Experience | flight time last 90 days : 250 flight time total : 1600 flight time type : 150 |
ASRS Report | 449692 |
Person 2 | |
Affiliation | other |
Function | instruction : trainee |
Qualification | pilot : private |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : fuel leak in cockpit other flight crewa other flight crewb |
Resolutory Action | aircraft : evacuated flight crew : declared emergency flight crew : landed in emergency condition |
Consequence | other other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
After departing bdr runway 24, my student and I detected a strong fuel odor in the cockpit. We decided to return for landing, and on downwind I noticed fuel pouring out from under the panel on the right side. I contacted the tower and asked them to roll the emergency equipment. After they received my response, I shut off the avionics and master switch and alternators. On 3/4 mi final, I shut off the fuel selectors, pulled the mixtures and shut off the magnetos. Once we rolled to a stop we exited the aircraft and ran away while the crash fire rescue equipment crew secured the scene. There was no fire or damage to the aircraft. Upon closer inspection by maintenance personnel, it was determined that a fuel line to the fuel pressure gauge was leaking at a fitting and loosened when takeoff power was applied. Being current in emergency procedures in the aircraft prevented the situation from becoming much worse. The development of newer technology to keep fuel lines out of the cockpit would also have helped the situation.
Original NASA ASRS Text
Title: INSTRUCTOR PLT, WITH STUDENT, OF A BEECH BE58 BARON DECLARED AN EMER AFTER TKOF AND RETURNED TO LAND DUE TO FUEL LEAKING INTO THE COCKPIT.
Narrative: AFTER DEPARTING BDR RWY 24, MY STUDENT AND I DETECTED A STRONG FUEL ODOR IN THE COCKPIT. WE DECIDED TO RETURN FOR LNDG, AND ON DOWNWIND I NOTICED FUEL POURING OUT FROM UNDER THE PANEL ON THE R SIDE. I CONTACTED THE TWR AND ASKED THEM TO ROLL THE EMER EQUIP. AFTER THEY RECEIVED MY RESPONSE, I SHUT OFF THE AVIONICS AND MASTER SWITCH AND ALTERNATORS. ON 3/4 MI FINAL, I SHUT OFF THE FUEL SELECTORS, PULLED THE MIXTURES AND SHUT OFF THE MAGNETOS. ONCE WE ROLLED TO A STOP WE EXITED THE ACFT AND RAN AWAY WHILE THE CFR CREW SECURED THE SCENE. THERE WAS NO FIRE OR DAMAGE TO THE ACFT. UPON CLOSER INSPECTION BY MAINT PERSONNEL, IT WAS DETERMINED THAT A FUEL LINE TO THE FUEL PRESSURE GAUGE WAS LEAKING AT A FITTING AND LOOSENED WHEN TKOF PWR WAS APPLIED. BEING CURRENT IN EMER PROCS IN THE ACFT PREVENTED THE SIT FROM BECOMING MUCH WORSE. THE DEVELOPMENT OF NEWER TECHNOLOGY TO KEEP FUEL LINES OUT OF THE COCKPIT WOULD ALSO HAVE HELPED THE SIT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.