37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 503439 |
Time | |
Date | 200103 |
Day | Mon |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : hnl.airport |
State Reference | HI |
Altitude | msl single value : 9000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : hnl.tracon |
Operator | common carrier : air carrier |
Make Model Name | L-1011 Tri-Star All Series |
Operating Under FAR Part | Part 121 |
Navigation In Use | other |
Flight Phase | climbout : intermediate altitude |
Route In Use | departure : on vectors |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | observation : company check pilot |
Qualification | pilot : atp |
Experience | flight time last 90 days : 160 flight time total : 24500 flight time type : 10000 |
ASRS Report | 503439 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : #1 engine vibration indication other flight crewa |
Resolutory Action | flight crew : diverted to another airport |
Consequence | other other |
Supplementary | |
Problem Areas | Flight Crew Human Performance Aircraft Cabin Crew Human Performance |
Primary Problem | Aircraft |
Narrative:
Passing 9000 ft, flight attendants complained of burning smell in the cabin. The flight engineer and myself started investigating the odor -- checking pack temperatures and electrical loads. Shortly after #1 engine high vibration illuminated and #1 engine shook the aircraft and sounded a loud bang, the crew initiated shutdown procedures immediately, but severe damage resulted from the turbine section coming apart. Fuel was dumped and a normal landing (engine out) was made in hnl.
Original NASA ASRS Text
Title: AN L1011 IN CLB AT 9000 FT EXPERIENCED #1 ENG HIGH VIBRATION THEN LOUD BANG CAUSED BY #1 ENG TURBINE FAILURE.
Narrative: PASSING 9000 FT, FLT ATTENDANTS COMPLAINED OF BURNING SMELL IN THE CABIN. THE FE AND MYSELF STARTED INVESTIGATING THE ODOR -- CHKING PACK TEMPS AND ELECTRICAL LOADS. SHORTLY AFTER #1 ENG HIGH VIBRATION ILLUMINATED AND #1 ENG SHOOK THE ACFT AND SOUNDED A LOUD BANG, THE CREW INITIATED SHUTDOWN PROCS IMMEDIATELY, BUT SEVERE DAMAGE RESULTED FROM THE TURBINE SECTION COMING APART. FUEL WAS DUMPED AND A NORMAL LNDG (ENG OUT) WAS MADE IN HNL.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.