37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 505817 |
Time | |
Date | 200103 |
Day | Sun |
Local Time Of Day | 0601 To 1200 |
Place | |
State Reference | FO |
Altitude | msl bound lower : 3550 msl bound upper : 6000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : mco.tower |
Operator | common carrier : air carrier |
Make Model Name | B767-300 and 300 ER |
Operating Under FAR Part | Part 121 |
Navigation In Use | other |
Flight Phase | descent : approach |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : relief pilot |
Qualification | pilot : atp |
ASRS Report | 505817 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time last 90 days : 200 flight time total : 3500 flight time type : 770 |
ASRS Report | 505193 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly |
Independent Detector | other flight crewa other flight crewb |
Resolutory Action | flight crew : overcame equipment problem flight crew : regained aircraft control |
Consequence | faa : investigated other other |
Factors | |
Maintenance | contributing factor : engineering procedure performance deficiency : scheduled maintenance |
Supplementary | |
Problem Areas | Weather Environmental Factor Flight Crew Human Performance |
Primary Problem | Aircraft |
Narrative:
Z during approach while configuring for landing I noticed that the aircraft was not responding to afdc panel IAS commands. The speed was increasing instead of decreasing as commanded. In an attempt to slow the aircraft deployed the speed brakes. After a short period the vertical instantaneous climb indicator went to 6000 dn. At that time I disconnected the ap and pulled on the yoke. The yoke would not move forward or aft. It was jammed. Then I applied anu stabilizer trim to arrest descent. Descent stopped at 3500 MSL. Returned to 4000 using stabilizer trim for pitch control. Announced to the captain that the aircraft was being flown with a jammed elevator-stabilizer trim only for pitch control. He then took control of the aircraft verified condition of elevator control and made the landing using approximately 13 anu units of stabilizer trim to maintain pitch altitude. Callback conversation with reporter revealed the following information: the reporter stated in configuring the aircraft for landing with the autopilot engaged the IAS was lowered on the autopilot control panel, but the aircraft speed up. The reporter said the autopilot was disengaged and the aircraft pitched over 6000 feet per minute. The reporter stated both pilots pulled on the yoke aircraft nose up, but could not recover elevator control. The reporter said the aircraft control was gained with the stabilizer trim. The reporter said on the ground the right hand elevator three power control unit compartments were full of ice preventing inputs to the elevator. The reporter stated the suspected cause was an auxiliary power unit inlet door seal that allowed water to run down into the elevator power unit compartments. Callback from acn 506193. The reporter stated the aircraft was parked for several hours prior to the flight in a torrential rainstorm. The reporter said the aircraft was dispatched for a ten-hour flight with the right elevator compartments full of water, which froze. The reporter said when the airplane was being configured for landing the IAS was selected for descent, but the aircraft speed increased. The reporter stated the autopilot was disconnected and the aircraft pitched over at a 6000 ft per minute rate of descent. The reporter said both pilots pulled back on the yoke with full force recorded on the digital flight recorder as 20 degrees of elevator deflection, but the elevator only moved 1 degree. The reporter said control was regained with stabilizer trim at 3550 ft and aircraft was returned to 3800 ft and then landed using 13 units of nose up stabilizer trim. The reporter stated that fortunately one of the crew was trained in the technique of landing with only stabilizer trim imputting small gradual changes. The reporter said investigation found water in the elevator power unit compartments and believes a deteriorated auxiliary power unit inlet door seal was the source of the water.
Original NASA ASRS Text
Title: A B767-300 ON APPROACH AT 4000 FT ON AUTOPILOT ACFT PITCH OVER AT 6000 FT FPM. CREW UNABLE TO MOVE ELEVATORS AND GAINED CONTROL WITH STABILIZER TRIM.
Narrative: Z DURING APPROACH WHILE CONFIGURING FOR LANDING I NOTICED THAT THE ACFT WAS NOT RESPONDING TO AFDC PANEL IAS COMMANDS. THE SPEED WAS INCREASING INSTEAD OF DECREASING AS COMMANDED. IN AN ATTEMPT TO SLOW THE ACFT DEPLOYED THE SPEED BRAKES. AFTER A SHORT PERIOD THE VERTICAL INSTANTANEOUS CLIMB INDICATOR WENT TO 6000 DN. AT THAT TIME I DISCONNECTED THE AP AND PULLED ON THE YOKE. THE YOKE WOULD NOT MOVE FORWARD OR AFT. IT WAS JAMMED. THEN I APPLIED ANU STAB TRIM TO ARREST DESCENT. DESCENT STOPPED AT 3500 MSL. RETURNED TO 4000 USING STAB TRIM FOR PITCH CONTROL. ANNOUNCED TO THE CAPT THAT THE ACFT WAS BEING FLOWN WITH A JAMMED ELEVATOR-STAB TRIM ONLY FOR PITCH CONTROL. HE THEN TOOK CONTROL OF THE ACFT VERIFIED CONDITION OF ELEVATOR CONTROL AND MADE THE LANDING USING APPROXIMATELY 13 ANU UNITS OF STAB TRIM TO MAINTAIN PITCH ALTITUDE. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING INFO: THE RPTR STATED IN CONFIGURING THE ACFT FOR LANDING WITH THE AUTOPILOT ENGAGED THE IAS WAS LOWERED ON THE AUTOPILOT CONTROL PANEL, BUT THE ACFT SPEED UP. THE RPTR SAID THE AUTOPILOT WAS DISENGAGED AND THE ACFT PITCHED OVER 6000 FEET PER MINUTE. THE RPTR STATED BOTH PILOTS PULLED ON THE YOKE ACFT NOSE UP, BUT COULD NOT RECOVER ELEVATOR CONTROL. THE RPTR SAID THE ACFT CONTROL WAS GAINED WITH THE STABILIZER TRIM. THE RPTR SAID ON THE GROUND THE RIGHT HAND ELEVATOR THREE POWER CONTROL UNIT COMPARTMENTS WERE FULL OF ICE PREVENTING INPUTS TO THE ELEVATOR. THE RPTR STATED THE SUSPECTED CAUSE WAS AN AUXILIARY POWER UNIT INLET DOOR SEAL THAT ALLOWED WATER TO RUN DOWN INTO THE ELEVATOR POWER UNIT COMPARTMENTS. CALLBACK FROM ACN 506193. THE RPTR STATED THE ACFT WAS PARKED FOR SEVERAL HOURS PRIOR TO THE FLIGHT IN A TORRENTIAL RAINSTORM. THE RPTR SAID THE ACFT WAS DISPATCHED FOR A TEN-HOUR FLIGHT WITH THE RIGHT ELEVATOR COMPARTMENTS FULL OF WATER, WHICH FROZE. THE RPTR SAID WHEN THE AIRPLANE WAS BEING CONFIGURED FOR LANDING THE IAS WAS SELECTED FOR DESCENT, BUT THE ACFT SPEED INCREASED. THE RPTR STATED THE AUTOPILOT WAS DISCONNECTED AND THE ACFT PITCHED OVER AT A 6000 FT PER MINUTE RATE OF DESCENT. THE RPTR SAID BOTH PILOTS PULLED BACK ON THE YOKE WITH FULL FORCE RECORDED ON THE DIGITAL FLIGHT RECORDER AS 20 DEGREES OF ELEVATOR DEFLECTION, BUT THE ELEVATOR ONLY MOVED 1 DEGREE. THE RPTR SAID CONTROL WAS REGAINED WITH STABILIZER TRIM AT 3550 FT AND ACFT WAS RETURNED TO 3800 FT AND THEN LANDED USING 13 UNITS OF NOSE UP STABILIZER TRIM. THE RPTR STATED THAT FORTUNATELY ONE OF THE CREW WAS TRAINED IN THE TECHNIQUE OF LANDING WITH ONLY STABILIZER TRIM IMPUTTING SMALL GRADUAL CHANGES. THE RPTR SAID INVESTIGATION FOUND WATER IN THE ELEVATOR POWER UNIT COMPARTMENTS AND BELIEVES A DETERIORATED AUXILIARY POWER UNIT INLET DOOR SEAL WAS THE SOURCE OF THE WATER.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.