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|
Attributes | |
ACN | 514703 |
Time | |
Date | 200106 |
Day | Sat |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : msp.airport |
State Reference | MN |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | VMC |
Weather Elements | Windshear |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : dfw.tower |
Operator | common carrier : air carrier |
Make Model Name | B727-200 |
Operating Under FAR Part | Part 121 |
Flight Phase | landing : roll |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time last 90 days : 150 flight time total : 7800 flight time type : 2500 |
ASRS Report | 514703 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Events | |
Anomaly | cabin event other conflict : ground critical inflight encounter other other anomaly other anomaly |
Independent Detector | other flight crewa |
Resolutory Action | none taken : insufficient time |
Consequence | other other other |
Supplementary | |
Problem Areas | Weather Airport Flight Crew Human Performance Aircraft |
Primary Problem | Flight Crew Human Performance |
Narrative:
Normal, stabilized approach to runway 30R in good VFR, daylight conditions. Very light chop, wind 250 degrees at 16-20 KTS. Developed high sink rate over threshold. Added considerable power but was unable to arrest sink rate. Aircraft touched down firm, bounced, and touched down normally. 2 flight attendants seated on aft jump seats reported back and neck pains and were taken to local clinic. Subsequent postflt revealed that 4 oxygen masks had come down and no other abnormalities. Runway 30R approach is over a riverbed and is known to produce sinks about 1/3 of a mi out. There was a slight sink at that position, but then the approach was stabilized until the threshold.
Original NASA ASRS Text
Title: A B727 FLC IS INVOLVED IN A HARD LNDG THAT CAUSED BACK AND NECK PAINS TO THE 2 FLT ATTENDANTS SEATED IN THE REAR JUMP SEATS AT MSP, MN.
Narrative: NORMAL, STABILIZED APCH TO RWY 30R IN GOOD VFR, DAYLIGHT CONDITIONS. VERY LIGHT CHOP, WIND 250 DEGS AT 16-20 KTS. DEVELOPED HIGH SINK RATE OVER THRESHOLD. ADDED CONSIDERABLE PWR BUT WAS UNABLE TO ARREST SINK RATE. ACFT TOUCHED DOWN FIRM, BOUNCED, AND TOUCHED DOWN NORMALLY. 2 FLT ATTENDANTS SEATED ON AFT JUMP SEATS RPTED BACK AND NECK PAINS AND WERE TAKEN TO LCL CLINIC. SUBSEQUENT POSTFLT REVEALED THAT 4 OXYGEN MASKS HAD COME DOWN AND NO OTHER ABNORMALITIES. RWY 30R APCH IS OVER A RIVERBED AND IS KNOWN TO PRODUCE SINKS ABOUT 1/3 OF A MI OUT. THERE WAS A SLIGHT SINK AT THAT POS, BUT THEN THE APCH WAS STABILIZED UNTIL THE THRESHOLD.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.