37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 517924 |
Time | |
Date | 200107 |
Day | Sat |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : fll.airport |
State Reference | FL |
Altitude | msl single value : 5500 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : mia.tracon |
Operator | common carrier : air carrier |
Make Model Name | B757 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Navigation In Use | other |
Flight Phase | climbout : intermediate altitude |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
ASRS Report | 517924 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other other : 3 |
Resolutory Action | controller : issued new clearance flight crew : landed in emergency condition flight crew : declared emergency flight crew : diverted to another airport |
Consequence | other other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
During climb approximately 5500 ft, the purser entered the cockpit and informed me that some overhead panels in the middle of the coach cabin were coming down. I told him we would attend to it when we were clear of the WX and above 10000 ft. He then returned to inform me that there was a crackling sound from the overhead panels, a loud air noise, and more panels coming down. I told him that we were diverting to miami. On final approach, he returned again to inform me of excessive condensation in the cabin. We turned off packs. I declared an emergency due to overweight landing (2000 pounds). Mechanics found large crack in the main overhead air conditioning duct. Aircraft removed from service.
Original NASA ASRS Text
Title: B757-200 CREW HAD AIR CONDITIONING DUCT FAILURE IN FLL CLASS E AIRSPACE.
Narrative: DURING CLB APPROX 5500 FT, THE PURSER ENTERED THE COCKPIT AND INFORMED ME THAT SOME OVERHEAD PANELS IN THE MIDDLE OF THE COACH CABIN WERE COMING DOWN. I TOLD HIM WE WOULD ATTEND TO IT WHEN WE WERE CLR OF THE WX AND ABOVE 10000 FT. HE THEN RETURNED TO INFORM ME THAT THERE WAS A CRACKLING SOUND FROM THE OVERHEAD PANELS, A LOUD AIR NOISE, AND MORE PANELS COMING DOWN. I TOLD HIM THAT WE WERE DIVERTING TO MIAMI. ON FINAL APCH, HE RETURNED AGAIN TO INFORM ME OF EXCESSIVE CONDENSATION IN THE CABIN. WE TURNED OFF PACKS. I DECLARED AN EMER DUE TO OVERWT LNDG (2000 LBS). MECHS FOUND LARGE CRACK IN THE MAIN OVERHEAD AIR CONDITIONING DUCT. ACFT REMOVED FROM SVC.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.