37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 522561 |
Time | |
Date | 200108 |
Day | Wed |
Place | |
Locale Reference | airport : lnk.airport |
State Reference | NE |
Altitude | msl single value : 35000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zmp.artcc |
Operator | general aviation : corporate |
Make Model Name | Learjet 55 |
Operating Under FAR Part | Part 91 |
Navigation In Use | other |
Flight Phase | cruise : level |
Route In Use | enroute : on vectors |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : corporate |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : cfi pilot : multi engine |
Experience | flight time last 90 days : 40 flight time total : 12500 flight time type : 5000 |
ASRS Report | 522561 |
Person 2 | |
Affiliation | company : corporate |
Function | flight crew : first officer |
Events | |
Anomaly | aircraft equipment problem : critical maintenance problem : improper maintenance other anomaly other |
Independent Detector | other flight crewa other flight crewb |
Resolutory Action | flight crew : overcame equipment problem |
Consequence | other |
Factors | |
Maintenance | performance deficiency : inspection performance deficiency : testing performance deficiency : repair performance deficiency : installation |
Supplementary | |
Problem Areas | Aircraft Maintenance Human Performance |
Primary Problem | Maintenance Human Performance |
Narrative:
During a flight after maintenance, we lost communications on both communications. We used our emergency handheld xceiver and established contact after approximately 5 mins. ATC said we had a stuck microphone. However, we had both transmitters set on different frequencys and still could not transmit or receive. This was a problem after maintenance on the ground run and was corrected by maintenance prior to this flight. After about 10 mins, the radios started working again. Maintenance found a bad pin in a connector.
Original NASA ASRS Text
Title: AN LJ55 CREW LOST ALL COMS FOR APPROX 10 MINS WHILE ON A TEST FLT FOLLOWING MAINT.
Narrative: DURING A FLT AFTER MAINT, WE LOST COMS ON BOTH COMS. WE USED OUR EMER HANDHELD XCEIVER AND ESTABLISHED CONTACT AFTER APPROX 5 MINS. ATC SAID WE HAD A STUCK MIKE. HOWEVER, WE HAD BOTH XMITTERS SET ON DIFFERENT FREQS AND STILL COULD NOT XMIT OR RECEIVE. THIS WAS A PROB AFTER MAINT ON THE GND RUN AND WAS CORRECTED BY MAINT PRIOR TO THIS FLT. AFTER ABOUT 10 MINS, THE RADIOS STARTED WORKING AGAIN. MAINT FOUND A BAD PIN IN A CONNECTOR.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.