37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 534046 |
Time | |
Date | 200201 |
Day | Thu |
Local Time Of Day | 0001 To 0600 |
Place | |
Locale Reference | airport : pdx.airport |
State Reference | OR |
Altitude | msl single value : 1500 |
Environment | |
Flight Conditions | VMC |
Light | Dawn |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | B737-300 |
Operating Under FAR Part | Part 121 |
Navigation In Use | other |
Flight Phase | climbout : initial |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : multi engine pilot : flight engineer pilot : commercial pilot : cfi pilot : atp pilot : instrument |
Experience | flight time last 90 days : 240 flight time total : 17000 flight time type : 11500 |
ASRS Report | 534046 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : nose gear light other flight crewa other flight crewb |
Resolutory Action | flight crew : landed as precaution |
Consequence | other other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
On takeoff from portland, or, (pdx) on runway 10L, I immediately noticed that the nose landing gear (red) unsafe light was illuminated, the aircraft was not pressurizing properly, and the noise level in the cockpit was exceptionally loud. (It was apparent that the nose wheel, or the nose gear door was not in the fully retracted position). After coordinating with our maintenance and dispatch department, and after attempting to recycle the landing gear, we decided to return to portland. After burning fuel down to landing weight, we returned to pdx and accomplished an ILS to runway 10R in visual conditions. Since all landing gear down indications were normal, hydraulic quantities and pressure were normal, and the nose gear was verified down and locked by the viewer port, no emergency was declared and an uneventful landing was accomplished. Postflt inspection revealed no damage, leaks, or pins installed. Aircraft turned over to company maintenance. Emergency equipment was called for by ATC, but was not needed.
Original NASA ASRS Text
Title: B737-300 FLC RETURNED TO LAND DUE TO AN UNSAFE NOSE GEAR RETRACTION PROB.
Narrative: ON TKOF FROM PORTLAND, OR, (PDX) ON RWY 10L, I IMMEDIATELY NOTICED THAT THE NOSE LNDG GEAR (RED) UNSAFE LIGHT WAS ILLUMINATED, THE ACFT WAS NOT PRESSURIZING PROPERLY, AND THE NOISE LEVEL IN THE COCKPIT WAS EXCEPTIONALLY LOUD. (IT WAS APPARENT THAT THE NOSE WHEEL, OR THE NOSE GEAR DOOR WAS NOT IN THE FULLY RETRACTED POSITION). AFTER COORDINATING WITH OUR MAINT AND DISPATCH DEPARTMENT, AND AFTER ATTEMPTING TO RECYCLE THE LNDG GEAR, WE DECIDED TO RETURN TO PORTLAND. AFTER BURNING FUEL DOWN TO LNDG WEIGHT, WE RETURNED TO PDX AND ACCOMPLISHED AN ILS TO RWY 10R IN VISUAL CONDITIONS. SINCE ALL LNDG GEAR DOWN INDICATIONS WERE NORMAL, HYDRAULIC QUANTITIES AND PRESSURE WERE NORMAL, AND THE NOSE GEAR WAS VERIFIED DOWN AND LOCKED BY THE VIEWER PORT, NO EMER WAS DECLARED AND AN UNEVENTFUL LNDG WAS ACCOMPLISHED. POSTFLT INSPECTION REVEALED NO DAMAGE, LEAKS, OR PINS INSTALLED. ACFT TURNED OVER TO COMPANY MAINT. EMER EQUIP WAS CALLED FOR BY ATC, BUT WAS NOT NEEDED.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.