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|
Attributes | |
ACN | 554490 |
Time | |
Date | 200207 |
Day | Sun |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : y47.airport |
State Reference | MI |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | general aviation : personal |
Make Model Name | Experimental |
Operating Under FAR Part | Part 91 |
Flight Phase | landing : roll |
Flight Plan | VFR |
Person 1 | |
Affiliation | other |
Function | flight crew : single pilot |
Qualification | pilot : commercial pilot : multi engine pilot : instrument |
Experience | flight time last 90 days : 67 flight time total : 2250 flight time type : 597 |
ASRS Report | 554490 |
Events | |
Anomaly | ground encounters other other anomaly other anomaly |
Independent Detector | other flight crewa |
Resolutory Action | none taken : anomaly accepted |
Consequence | other other |
Supplementary | |
Problem Areas | Aircraft Flight Crew Human Performance |
Primary Problem | Flight Crew Human Performance |
Narrative:
This incident was caused by overconfidence on my part. I had become too complacent in flying (landing) the airplane. I will not do this again. As I see this incident, 4 problems occurred. A go around could have been made at any one of these 4 points: 1) I turned final too high. 2) I descended at 2000 FPM. The descent rate was too steep. 3) I did not arrest the descent quickly enough. The aircraft bounced, but no damage occurred. 4) rather than go around, I attempted to salvage the landing. The aircraft stalled at about 10 ft AGL. The left main gear hit first. The right main gear followed, but hit harder. The nose then came down hard enough to compress the nose strut and cause the propeller to hit the runway. Looking at the runway after the fact, 7 blade marks could be seen. The only damage to the aircraft was a bent propeller, a bent right main strut and a bent nose gear fork. The plane was still taxiable.
Original NASA ASRS Text
Title: AN LNC2-I (LANCAIR) PLT, EXPERIENCED A HARD DAMAGING LNDG WHILE TRYING TO SALVAGE A NON DAMAGING BOUNCE.
Narrative: THIS INCIDENT WAS CAUSED BY OVERCONFIDENCE ON MY PART. I HAD BECOME TOO COMPLACENT IN FLYING (LNDG) THE AIRPLANE. I WILL NOT DO THIS AGAIN. AS I SEE THIS INCIDENT, 4 PROBS OCCURRED. A GAR COULD HAVE BEEN MADE AT ANY ONE OF THESE 4 POINTS: 1) I TURNED FINAL TOO HIGH. 2) I DSNDED AT 2000 FPM. THE DSCNT RATE WAS TOO STEEP. 3) I DID NOT ARREST THE DSCNT QUICKLY ENOUGH. THE ACFT BOUNCED, BUT NO DAMAGE OCCURRED. 4) RATHER THAN GO AROUND, I ATTEMPTED TO SALVAGE THE LNDG. THE ACFT STALLED AT ABOUT 10 FT AGL. THE L MAIN GEAR HIT FIRST. THE R MAIN GEAR FOLLOWED, BUT HIT HARDER. THE NOSE THEN CAME DOWN HARD ENOUGH TO COMPRESS THE NOSE STRUT AND CAUSE THE PROP TO HIT THE RWY. LOOKING AT THE RWY AFTER THE FACT, 7 BLADE MARKS COULD BE SEEN. THE ONLY DAMAGE TO THE ACFT WAS A BENT PROP, A BENT R MAIN STRUT AND A BENT NOSE GEAR FORK. THE PLANE WAS STILL TAXIABLE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.