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|
Attributes | |
ACN | 557754 |
Time | |
Date | 200208 |
Day | Sat |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : fdk.airport |
State Reference | MD |
Altitude | agl bound lower : 0 agl bound upper : 300 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | general aviation : personal |
Make Model Name | Small Aircraft |
Operating Under FAR Part | Part 91 |
Flight Phase | climbout : takeoff cruise : level cruise : holding |
Flight Plan | None |
Aircraft 2 | |
Operator | general aviation : personal |
Make Model Name | Small Aircraft |
Operating Under FAR Part | Part 91 |
Flight Phase | cruise : level cruise : holding |
Flight Plan | None |
Person 1 | |
Affiliation | other |
Function | flight crew : single pilot |
Qualification | pilot : instrument pilot : private |
Experience | flight time last 90 days : 10 flight time total : 1750 flight time type : 250 |
ASRS Report | 557754 |
Person 2 | |
Affiliation | other |
Function | flight crew : single pilot |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : landed in emergency condition |
Consequence | other other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
We were in a race track pattern with all the l-baids at 300 ft, pt's and trainers at 500 ft, and faska trainers bt's, T6's at 700 ft during the airshow. Preflight briefing was completed. Taxi and run-up completed with no indications of rough engine seen. After making takeoff and 1 circuit around, the engine began to lose power and within 10 seconds quit. I made a dead stick landing back on runway 5 downwind. No damage to plane. Looks like oil pump failed or stuck valves.
Original NASA ASRS Text
Title: PLT OF A RACING T CRAFT L2M PERFORMS A FORCED EMER DOWNWIND LNDG DURING AN AIR RACE AT FDK, MD.
Narrative: WE WERE IN A RACE TRACK PATTERN WITH ALL THE L-BAIDS AT 300 FT, PT'S AND TRAINERS AT 500 FT, AND FASKA TRAINERS BT'S, T6'S AT 700 FT DURING THE AIRSHOW. PREFLT BRIEFING WAS COMPLETED. TAXI AND RUN-UP COMPLETED WITH NO INDICATIONS OF ROUGH ENG SEEN. AFTER MAKING TKOF AND 1 CIRCUIT AROUND, THE ENG BEGAN TO LOSE PWR AND WITHIN 10 SECONDS QUIT. I MADE A DEAD STICK LNDG BACK ON RWY 5 DOWNWIND. NO DAMAGE TO PLANE. LOOKS LIKE OIL PUMP FAILED OR STUCK VALVES.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.