37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 559661 |
Time | |
Date | 200210 |
Day | Tue |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : zzzz.airport |
State Reference | FO |
Altitude | agl single value : 0 |
Environment | |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Fokker 100 |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : maintenance |
Person 1 | |
Affiliation | company : air carrier |
Function | maintenance : technician |
Qualification | technician : powerplant technician : airframe |
ASRS Report | 559661 |
Person 2 | |
Affiliation | company : air carrier |
Function | other personnel other |
Events | |
Anomaly | aircraft equipment problem : critical maintenance problem : improper maintenance maintenance problem : improper documentation non adherence : far non adherence : published procedure |
Independent Detector | aircraft equipment other aircraft equipment : oil filter bypass warning other flight crewa other flight crewb |
Resolutory Action | flight crew : diverted to another airport |
Consequence | other other |
Factors | |
Maintenance | contributing factor : schedule pressure contributing factor : manuals performance deficiency : logbook entry performance deficiency : testing performance deficiency : non compliance with legal requirements |
Supplementary | |
Problem Areas | Maintenance Human Performance Chart Or Publication Aircraft |
Primary Problem | Maintenance Human Performance |
Narrative:
Accomplished the maintenance procedures manual 79-02. I disconnected, by mistake, the wrong connector. Was engine oil filter differential pressure instead of engine oil pressure transmitter. So the plane returned back to the gate. I made contact with ZZZ1 technician. They told me to rechk the cannon. I did -- it was the wrong connector.
Original NASA ASRS Text
Title: A FOKKER 100 WAS DISPATCHED IN NON COMPLIANCE WITH THE ENG OIL FILTER BYPASS CONNECTOR XMITTER CONNECTOR.
Narrative: ACCOMPLISHED THE MAINT PROCS MANUAL 79-02. I DISCONNECTED, BY MISTAKE, THE WRONG CONNECTOR. WAS ENG OIL FILTER DIFFERENTIAL PRESSURE INSTEAD OF ENG OIL PRESSURE XMITTER. SO THE PLANE RETURNED BACK TO THE GATE. I MADE CONTACT WITH ZZZ1 TECHNICIAN. THEY TOLD ME TO RECHK THE CANNON. I DID -- IT WAS THE WRONG CONNECTOR.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.