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|
Attributes | |
ACN | 573859 |
Time | |
Date | 200302 |
Day | Mon |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : pit.airport |
State Reference | PA |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | MD-88 |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : taxi ground : takeoff roll |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : instrument pilot : multi engine |
Experience | flight time last 90 days : 220 flight time total : 9820 flight time type : 6300 |
ASRS Report | 573859 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Events | |
Anomaly | aircraft equipment problem : critical maintenance problem : improper documentation maintenance problem : non compliance with mel non adherence : company policies non adherence : far |
Independent Detector | other flight crewa other flight crewb |
Resolutory Action | flight crew : diverted to another airport other |
Consequence | other other other |
Supplementary | |
Problem Areas | Flight Crew Human Performance Aircraft |
Primary Problem | Aircraft |
Narrative:
After deicing and taxi to runway 10C, the left generator dropped off-line. Complied with MEL and the left bus was pwred by APU. At approximately V1, the right generator dropped off-line. Climbed to 5000 ft, leveled off and turned downwind. Per abnormal procedures checklist, the right generator would not reset and the right bus load picked up by the APU. Executed an uneventful landing and returned to gate. Problem: faulty electrical system. Problem: not informing flight dispatch of situation with left generator on the ground (prior to takeoff). Problem: improper write-up in logbook (postflt). Corrective actions: 1) inform dispatch of all sits prior to takeoff. 2) insure write-up is actually the occurrence that happened in the proper time line.
Original NASA ASRS Text
Title: AFTER LOSING THE L GENERATOR AND SUPPLEMENTING REQUIREMENTS WITH THE APU, AN MD88 FLT CREW LOSES ITS SECOND GENERATOR AT V1 AND AFTER TKOF RETURNS/LANDS AT PIT, PA.
Narrative: AFTER DEICING AND TAXI TO RWY 10C, THE L GENERATOR DROPPED OFF-LINE. COMPLIED WITH MEL AND THE L BUS WAS PWRED BY APU. AT APPROX V1, THE R GENERATOR DROPPED OFF-LINE. CLBED TO 5000 FT, LEVELED OFF AND TURNED DOWNWIND. PER ABNORMAL PROCS CHKLIST, THE R GENERATOR WOULD NOT RESET AND THE R BUS LOAD PICKED UP BY THE APU. EXECUTED AN UNEVENTFUL LNDG AND RETURNED TO GATE. PROB: FAULTY ELECTRICAL SYS. PROB: NOT INFORMING FLT DISPATCH OF SIT WITH L GENERATOR ON THE GND (PRIOR TO TKOF). PROB: IMPROPER WRITE-UP IN LOGBOOK (POSTFLT). CORRECTIVE ACTIONS: 1) INFORM DISPATCH OF ALL SITS PRIOR TO TKOF. 2) INSURE WRITE-UP IS ACTUALLY THE OCCURRENCE THAT HAPPENED IN THE PROPER TIME LINE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.