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|
Attributes | |
ACN | 622384 |
Time | |
Date | 200401 |
Day | Mon |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : ord.airport |
State Reference | IL |
Altitude | msl single value : 2500 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tracon : c90.tracon |
Operator | common carrier : air carrier |
Make Model Name | B737 Undifferentiated or Other Model |
Operating Under FAR Part | Part 121 |
Flight Phase | descent : approach |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Experience | flight time last 90 days : 200 flight time total : 14500 flight time type : 4500 |
ASRS Report | 622384 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Events | |
Anomaly | aircraft equipment problem : critical inflight encounter : birds other anomaly |
Independent Detector | other flight crewa other flight crewb |
Resolutory Action | flight crew : overcame equipment problem |
Consequence | other other |
Supplementary | |
Problem Areas | Environmental Factor |
Primary Problem | Environmental Factor |
Narrative:
We flew through a flock of very large birds (geese?) just outside the OM. We heard a few 'thumps' and knew that we hit at least 1 or 2. The autoplt was disconnected to make sure there was no control ability problem. The landing gear was then lowered to ensure that there was no problem getting the gear down and locked, which there wasn't. At about 500 ft AGL, the #2 engine was increased to about 43-44% N1. A compressor stall was felt along with vibration. The power lever was reduced, keeping the #2 engine below 42%. The landing was without incident, other than a very noticeable burning smell in the cabin. The #2 engine was shut down after clearing the runway. Postflt inspection showed bird ingestion in #2 engine with a lot of feathers and remains noted on the engine inlet.
Original NASA ASRS Text
Title: B737 CREW HAD MULTIPLE BIRD STRIKES ON APCH. THE ACFT ENG WAS DAMAGED.
Narrative: WE FLEW THROUGH A FLOCK OF VERY LARGE BIRDS (GEESE?) JUST OUTSIDE THE OM. WE HEARD A FEW 'THUMPS' AND KNEW THAT WE HIT AT LEAST 1 OR 2. THE AUTOPLT WAS DISCONNECTED TO MAKE SURE THERE WAS NO CTL ABILITY PROB. THE LNDG GEAR WAS THEN LOWERED TO ENSURE THAT THERE WAS NO PROB GETTING THE GEAR DOWN AND LOCKED, WHICH THERE WASN'T. AT ABOUT 500 FT AGL, THE #2 ENG WAS INCREASED TO ABOUT 43-44% N1. A COMPRESSOR STALL WAS FELT ALONG WITH VIBRATION. THE PWR LEVER WAS REDUCED, KEEPING THE #2 ENG BELOW 42%. THE LNDG WAS WITHOUT INCIDENT, OTHER THAN A VERY NOTICEABLE BURNING SMELL IN THE CABIN. THE #2 ENG WAS SHUT DOWN AFTER CLRING THE RWY. POSTFLT INSPECTION SHOWED BIRD INGESTION IN #2 ENG WITH A LOT OF FEATHERS AND REMAINS NOTED ON THE ENG INLET.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.