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|
Attributes | |
ACN | 654327 |
Time | |
Date | 200504 |
Place | |
Locale Reference | airport : zzz.airport |
State Reference | US |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tower : zzz.tower |
Operator | general aviation : personal |
Make Model Name | Cessna 150 |
Operating Under FAR Part | Part 91 |
Flight Phase | ground : takeoff roll |
Flight Plan | None |
Person 1 | |
Affiliation | other |
Function | flight crew : single pilot |
Qualification | pilot : cfi pilot : commercial pilot : instrument pilot : multi engine technician : powerplant technician : airframe |
Experience | flight time last 90 days : 45 flight time total : 2900 flight time type : 1500 maintenance repairman : 11 |
ASRS Report | 654327 |
Person 2 | |
Affiliation | other |
Function | maintenance : technician |
Qualification | technician : powerplant technician : inspection authority technician : airframe |
ASRS Report | 654408 |
Events | |
Anomaly | aircraft equipment problem : critical maintenance problem : improper maintenance maintenance problem : improper documentation non adherence : far non adherence : published procedure |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : rejected takeoff |
Consequence | other |
Factors | |
Maintenance | performance deficiency : inspection performance deficiency : installation performance deficiency : non compliance with legal requirements performance deficiency : scheduled maintenance |
Supplementary | |
Problem Areas | Maintenance Human Performance Aircraft Environmental Factor |
Primary Problem | Maintenance Human Performance |
Narrative:
I was taking off from ZZZ when I experienced a loss of power. I told the tower that I was aborting takeoff and canceled my clearance and taxied to parking. I could not determine the cause but in a further run-up; the engine made full power so I assumed the problem was possibly too lean a mixture and so called for another clearance. As I was taxiing out; I thought that I had hit a chock with my nosewheel but it was later determined that the line men had left it standing on its end instead of laying flat and the tip of my propeller had hit it. Since I did not have reason to believe the nose gear was damaged; I attempted another takeoff and again experienced a power loss and so taxied back and had a mechanic look at it and it was determined that a cotter key had somehow come out of the nut holding the carburetor arm and it came loose enough to cause intermittent slipping when the throttle was pushed to the full on position. The mechanic repaired the problem using cessna's procedures and I flew back home. That night I got a call from an FAA inspector and I told him the story and he said that we have a maintenance issue and that he would be calling me the following week. Supplemental information from acn 654408: the last annual inspection was completed two weeks ago. The engine controls were checked and inspected at that time.
Original NASA ASRS Text
Title: A C150 ABORTED TKOF TWICE DUE TO LOSS OF PWR. FOUND CARB CTL ARM LOOSE. LOCK NUT BACKED OFF DUE TO LOSS OF COTTER PIN.
Narrative: I WAS TAKING OFF FROM ZZZ WHEN I EXPERIENCED A LOSS OF PWR. I TOLD THE TWR THAT I WAS ABORTING TKOF AND CANCELED MY CLRNC AND TAXIED TO PARKING. I COULD NOT DETERMINE THE CAUSE BUT IN A FURTHER RUN-UP; THE ENG MADE FULL PWR SO I ASSUMED THE PROB WAS POSSIBLY TOO LEAN A MIXTURE AND SO CALLED FOR ANOTHER CLRNC. AS I WAS TAXIING OUT; I THOUGHT THAT I HAD HIT A CHOCK WITH MY NOSEWHEEL BUT IT WAS LATER DETERMINED THAT THE LINE MEN HAD LEFT IT STANDING ON ITS END INSTEAD OF LAYING FLAT AND THE TIP OF MY PROP HAD HIT IT. SINCE I DID NOT HAVE REASON TO BELIEVE THE NOSE GEAR WAS DAMAGED; I ATTEMPTED ANOTHER TKOF AND AGAIN EXPERIENCED A PWR LOSS AND SO TAXIED BACK AND HAD A MECH LOOK AT IT AND IT WAS DETERMINED THAT A COTTER KEY HAD SOMEHOW COME OUT OF THE NUT HOLDING THE CARB ARM AND IT CAME LOOSE ENOUGH TO CAUSE INTERMITTENT SLIPPING WHEN THE THROTTLE WAS PUSHED TO THE FULL ON POS. THE MECH REPAIRED THE PROB USING CESSNA'S PROCS AND I FLEW BACK HOME. THAT NIGHT I GOT A CALL FROM AN FAA INSPECTOR AND I TOLD HIM THE STORY AND HE SAID THAT WE HAVE A MAINT ISSUE AND THAT HE WOULD BE CALLING ME THE FOLLOWING WK. SUPPLEMENTAL INFO FROM ACN 654408: THE LAST ANNUAL INSPECTION WAS COMPLETED TWO WEEKS AGO. THE ENG CTLS WERE CHECKED AND INSPECTED AT THAT TIME.
Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.