Narrative:

After performing a repositioning of a fuel control rod; the discrepancy was signed off and the aircraft pushed back. After #2 engine had been started by the flight crew and they were starting #3 engine; the #2 engine went to high thrust and caused the aircraft to overpwr the tug. This resulted in the aircraft breaking the tow bar and striking the tug; causing severe damage to the aircraft. No personnel were injured and the crew shut the engine down.

Google
 

Original NASA ASRS Text

Title: A B727 ON PUSHBACK STARTED #2 ENG WHICH WENT TO FULL PWR UNCOMMANDED. AIRPLANE SNAPPED THE TOW BAR AND STRUCK THE TUG; INCURRING SEVERE DAMAGE.

Narrative: AFTER PERFORMING A REPOSITIONING OF A FUEL CTL ROD; THE DISCREPANCY WAS SIGNED OFF AND THE ACFT PUSHED BACK. AFTER #2 ENG HAD BEEN STARTED BY THE FLT CREW AND THEY WERE STARTING #3 ENG; THE #2 ENG WENT TO HIGH THRUST AND CAUSED THE ACFT TO OVERPWR THE TUG. THIS RESULTED IN THE ACFT BREAKING THE TOW BAR AND STRIKING THE TUG; CAUSING SEVERE DAMAGE TO THE ACFT. NO PERSONNEL WERE INJURED AND THE CREW SHUT THE ENG DOWN.

Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.