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|
Attributes | |
ACN | 691880 |
Time | |
Date | 200603 |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : zzz.airport |
State Reference | US |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zzz.artcc |
Operator | common carrier : charter |
Make Model Name | King Air C90 E90 |
Operating Under FAR Part | Part 135 |
Flight Phase | cruise : level |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : charter |
Function | flight crew : single pilot oversight : pic |
Qualification | pilot : multi engine pilot : private pilot : instrument pilot : commercial |
Experience | flight time last 90 days : 14 flight time total : 1627 flight time type : 337 |
ASRS Report | 691880 |
Events | |
Anomaly | aircraft equipment problem : critical maintenance problem : improper maintenance |
Independent Detector | aircraft equipment other aircraft equipment : oil pressure gauge other flight crewa |
Resolutory Action | flight crew : diverted to another airport flight crew : landed as precaution |
Consequence | other |
Supplementary | |
Problem Areas | Flight Crew Human Performance Maintenance Human Performance |
Primary Problem | Flight Crew Human Performance |
Narrative:
While en route; I noticed a fluctuation in torque on the right engine. I pulled the circuit breaker and reset it. Upon resetting the breaker; the torque continued to fluctuate. I scanned the other engine instruments to find low oil pressure in the right engine. I looked out to the right engine and noticed oil on the cowl and wing. I proceeded with the emergency engine shutdown procedure. I informed the passenger of the situation and then I proceeded to declare an emergency and change my destination. I shut the right engine down and the approach and landing were uneventful. I taxied to the ramp on the remaining engine. After deplaning and upon further examination of the engine. I noticed oil covering the surface of the cowling; wheel well; and engine. A possible cause of the oil leak was the improper placement of the oil dipstick. The dipstick was not sealed properly. A lineman had put a quart of oil in the right engine; secured the cowl and departed. On my way to examine the dipstick and cowl; my passenger arrived; not giving me the opportunity to rechk the lineman's work.
Original NASA ASRS Text
Title: BEECH KINGAIR 90 PLT HAS A PRECAUTIONARY ENG SHUTDOWN DUE TO LOSS OF ENG OIL.
Narrative: WHILE ENRTE; I NOTICED A FLUCTUATION IN TORQUE ON THE R ENG. I PULLED THE CIRCUIT BREAKER AND RESET IT. UPON RESETTING THE BREAKER; THE TORQUE CONTINUED TO FLUCTUATE. I SCANNED THE OTHER ENG INSTS TO FIND LOW OIL PRESSURE IN THE R ENG. I LOOKED OUT TO THE R ENG AND NOTICED OIL ON THE COWL AND WING. I PROCEEDED WITH THE EMER ENG SHUTDOWN PROC. I INFORMED THE PAX OF THE SITUATION AND THEN I PROCEEDED TO DECLARE AN EMER AND CHANGE MY DEST. I SHUT THE R ENG DOWN AND THE APCH AND LNDG WERE UNEVENTFUL. I TAXIED TO THE RAMP ON THE REMAINING ENG. AFTER DEPLANING AND UPON FURTHER EXAMINATION OF THE ENG. I NOTICED OIL COVERING THE SURFACE OF THE COWLING; WHEEL WELL; AND ENG. A POSSIBLE CAUSE OF THE OIL LEAK WAS THE IMPROPER PLACEMENT OF THE OIL DIPSTICK. THE DIPSTICK WAS NOT SEALED PROPERLY. A LINEMAN HAD PUT A QUART OF OIL IN THE R ENG; SECURED THE COWL AND DEPARTED. ON MY WAY TO EXAMINE THE DIPSTICK AND COWL; MY PAX ARRIVED; NOT GIVING ME THE OPPORTUNITY TO RECHK THE LINEMAN'S WORK.
Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.