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|
Attributes | |
ACN | 717637 |
Time | |
Date | 200611 |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : dfw.airport |
State Reference | TX |
Altitude | agl bound lower : 1500 agl bound upper : 2500 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : d10.tracon |
Operator | common carrier : air carrier |
Make Model Name | MD-10 Conversion |
Operating Under FAR Part | Part 121 |
Navigation In Use | other |
Flight Phase | climbout : takeoff climbout : initial |
Route In Use | departure sid : soldo |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : multi engine pilot : instrument pilot : commercial pilot : atp |
Experience | flight time last 90 days : 50 flight time total : 4000 flight time type : 62 |
ASRS Report | 717637 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Events | |
Anomaly | aircraft equipment problem : less severe non adherence : published procedure non adherence : far non adherence : clearance other spatial deviation |
Independent Detector | other controllera other flight crewa |
Resolutory Action | controller : issued advisory flight crew : returned to intended or assigned course |
Consequence | faa : investigated |
Supplementary | |
Problem Areas | Flight Crew Human Performance Chart Or Publication Airspace Structure Aircraft |
Primary Problem | Ambiguous |
Narrative:
We took off on runway 17C from dfw on the soldo departure. With navigation engaged; just after takeoff and after I had engaged the autoplt and 'prof;' the aircraft started turning left. I realized that something was wrong with the navigation. The navigation display showed the next waypoint as soldo; which was wrong. The waypoint that we should have been navigating to was trexx; which is basically straight ahead. I 'heading selected' us to the correct heading. That correction wasn't happening fast enough; so I disconnected the autoplt; and brought us back towards the correct heading. Just as we were settling on the heading (and simultaneously the first officer was trying to put trexx back into the FMS) we had several things happen. We got a master caution light for engine #3 anti-ice disagreement alert. About the same time the flaps were up and we were well above flap retract speed; but we got a momentary stick shaker. And my (the captain's) headset came unplugged. Dfw departure told us to come left to 090 degrees. They then said there was a course deviation and we should call them when we landed. Upon landing and talking to dfw TRACON; they said that there had been another flight taking off from the runways 18 (western runways at dfw) and we had come within 2.14 mi and 700 ft vertically. Bottom line: we were distraction by aircraft mechanical issues at a critical time and we overshot our correction to the outbound course (174 degrees to trexx). I am not sure why the incorrect waypoint sequenced in the FMS. Had we been navigating correctly to trexx; this would not have occurred. However; once the initial (incorrect) turn towards soldo occurred; we should have immediately called ATC and notified them. As it was; a few seconds delay during the correction then put us into a situation that distraction us further with aircraft mechanical issues. Had we immediately called ATC at the first hint of a navigation problem; they likely would have helped prevent us from deviating back past the course line to the west and prevented the conflict.
Original NASA ASRS Text
Title: AN MD10 ON THE DFW RWY 17C SOLDO 2 RNAV DEP DEVIATED WHEN THE FMS ATTEMPTED DIRECT SOLDO 2 INTXN BYPASSING INTERMEDIATE INTXNS.
Narrative: WE TOOK OFF ON RWY 17C FROM DFW ON THE SOLDO DEP. WITH NAV ENGAGED; JUST AFTER TKOF AND AFTER I HAD ENGAGED THE AUTOPLT AND 'PROF;' THE ACFT STARTED TURNING L. I REALIZED THAT SOMETHING WAS WRONG WITH THE NAV. THE NAV DISPLAY SHOWED THE NEXT WAYPOINT AS SOLDO; WHICH WAS WRONG. THE WAYPOINT THAT WE SHOULD HAVE BEEN NAVING TO WAS TREXX; WHICH IS BASICALLY STRAIGHT AHEAD. I 'HDG SELECTED' US TO THE CORRECT HDG. THAT CORRECTION WASN'T HAPPENING FAST ENOUGH; SO I DISCONNECTED THE AUTOPLT; AND BROUGHT US BACK TOWARDS THE CORRECT HDG. JUST AS WE WERE SETTLING ON THE HDG (AND SIMULTANEOUSLY THE FO WAS TRYING TO PUT TREXX BACK INTO THE FMS) WE HAD SEVERAL THINGS HAPPEN. WE GOT A MASTER CAUTION LIGHT FOR ENG #3 ANTI-ICE DISAGREEMENT ALERT. ABOUT THE SAME TIME THE FLAPS WERE UP AND WE WERE WELL ABOVE FLAP RETRACT SPD; BUT WE GOT A MOMENTARY STICK SHAKER. AND MY (THE CAPT'S) HEADSET CAME UNPLUGGED. DFW DEP TOLD US TO COME L TO 090 DEGS. THEY THEN SAID THERE WAS A COURSE DEV AND WE SHOULD CALL THEM WHEN WE LANDED. UPON LNDG AND TALKING TO DFW TRACON; THEY SAID THAT THERE HAD BEEN ANOTHER FLT TAKING OFF FROM THE RWYS 18 (WESTERN RWYS AT DFW) AND WE HAD COME WITHIN 2.14 MI AND 700 FT VERTICALLY. BOTTOM LINE: WE WERE DISTR BY ACFT MECHANICAL ISSUES AT A CRITICAL TIME AND WE OVERSHOT OUR CORRECTION TO THE OUTBOUND COURSE (174 DEGS TO TREXX). I AM NOT SURE WHY THE INCORRECT WAYPOINT SEQUENCED IN THE FMS. HAD WE BEEN NAVING CORRECTLY TO TREXX; THIS WOULD NOT HAVE OCCURRED. HOWEVER; ONCE THE INITIAL (INCORRECT) TURN TOWARDS SOLDO OCCURRED; WE SHOULD HAVE IMMEDIATELY CALLED ATC AND NOTIFIED THEM. AS IT WAS; A FEW SECONDS DELAY DURING THE CORRECTION THEN PUT US INTO A SITUATION THAT DISTR US FURTHER WITH ACFT MECHANICAL ISSUES. HAD WE IMMEDIATELY CALLED ATC AT THE FIRST HINT OF A NAV PROB; THEY LIKELY WOULD HAVE HELPED PREVENT US FROM DEVIATING BACK PAST THE COURSE LINE TO THE W AND PREVENTED THE CONFLICT.
Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.