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|
Attributes | |
ACN | 720389 |
Time | |
Date | 200612 |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : smf.airport |
State Reference | CA |
Altitude | msl single value : 1000 |
Environment | |
Flight Conditions | VMC |
Aircraft 1 | |
Controlling Facilities | tracon : nct.tracon |
Operator | common carrier : air carrier |
Make Model Name | B737-300 |
Operating Under FAR Part | Part 121 |
Navigation In Use | other |
Flight Phase | climbout : takeoff |
Route In Use | departure sid : frogo6.frogo |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Experience | flight time last 90 days : 210 flight time type : 1600 |
ASRS Report | 720389 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Experience | flight time last 90 days : 214 |
ASRS Report | 719833 |
Events | |
Anomaly | aircraft equipment problem : less severe other anomaly |
Independent Detector | other flight crewa |
Resolutory Action | none taken : detected after the fact |
Consequence | other |
Supplementary | |
Problem Areas | Aircraft Flight Crew Human Performance |
Primary Problem | Flight Crew Human Performance |
Narrative:
While on initial climb out on the frogo 6 departure from sacramento airport; and immediately following 'flaps 1' callout and execution; received amended clearance from ATC. We were cleared direct frogo and received a frequency change. As the pilot monitoring I loaded the direct frogo in the FMC and as I finished I noticed a large bird fly by the right side of the aircraft and called it out to the PF. The captain had his attention on the takeoff as well as the WX painting on the radar. We referenced the engine instruments to verify no bird strike occurred on the right engine. It was at that moment the captain realized the flaps were still as position 1. He immediately called for flaps up; but not before we noticed that the airspeed was 235 KTS. The flaps were retracted and no further incidence occurred. We called in for maintenance at our arrival city and an inspection of the flaps revealed no damage. Remainder of flts were uneventful. Better vigilance by both crew members in ensuring checklist items are accomplished in a timely manner.
Original NASA ASRS Text
Title: B737 CREW GETS DISTR DURING DEP AND OVERSPDS FLAPS.
Narrative: WHILE ON INITIAL CLBOUT ON THE FROGO 6 DEP FROM SACRAMENTO ARPT; AND IMMEDIATELY FOLLOWING 'FLAPS 1' CALLOUT AND EXECUTION; RECEIVED AMENDED CLRNC FROM ATC. WE WERE CLRED DIRECT FROGO AND RECEIVED A FREQ CHANGE. AS THE PLT MONITORING I LOADED THE DIRECT FROGO IN THE FMC AND AS I FINISHED I NOTICED A LARGE BIRD FLY BY THE R SIDE OF THE ACFT AND CALLED IT OUT TO THE PF. THE CAPT HAD HIS ATTN ON THE TKOF AS WELL AS THE WX PAINTING ON THE RADAR. WE REFED THE ENG INSTS TO VERIFY NO BIRD STRIKE OCCURRED ON THE R ENG. IT WAS AT THAT MOMENT THE CAPT REALIZED THE FLAPS WERE STILL AS POS 1. HE IMMEDIATELY CALLED FOR FLAPS UP; BUT NOT BEFORE WE NOTICED THAT THE AIRSPD WAS 235 KTS. THE FLAPS WERE RETRACTED AND NO FURTHER INCIDENCE OCCURRED. WE CALLED IN FOR MAINT AT OUR ARR CITY AND AN INSPECTION OF THE FLAPS REVEALED NO DAMAGE. REMAINDER OF FLTS WERE UNEVENTFUL. BETTER VIGILANCE BY BOTH CREW MEMBERS IN ENSURING CHKLIST ITEMS ARE ACCOMPLISHED IN A TIMELY MANNER.
Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.