Narrative:

Normal preflight; brief and startup for departure. Captain's leg was PF. Began takeoff roll on runway 17R at okc. At around 50 KIAS; a 'whistling/screeching' sound was noticed in the cockpit. Initially; crew thought it was due to possible pressurization sealing at high power. Going through 80 KIAS; noise became increasingly louder and sounded like something was grinding. Between 80-100 KIAS captain initiated rejected takeoff maneuver. Maneuver was performed perfectly with aircraft on centerline; call to flight attendants to remain seated; and tower to roll the trucks for brake inspection. Subsequently; crew cancelled request for emergency vehicles as there were no other indications of a problem; and the noise subsided. Taxied back to the ramp; deplaned; and contacted maintenance control. External inspection of the aircraft provided no indications of problem. Jumpseating flight attendant suggested that it sounded like an audio system malfunction -- which is what it ended up being. Boarding music system had inadvertently switched on with full volume and almost unbearable 'hiss/screech' in the cabin. Maintenance deferred the system and flight proceeded without further incident.

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Original NASA ASRS Text

Title: B737-300 FLT CREW HAS A REJECTED TKOF AT OKC.

Narrative: NORMAL PREFLT; BRIEF AND STARTUP FOR DEP. CAPT'S LEG WAS PF. BEGAN TKOF ROLL ON RWY 17R AT OKC. AT AROUND 50 KIAS; A 'WHISTLING/SCREECHING' SOUND WAS NOTICED IN THE COCKPIT. INITIALLY; CREW THOUGHT IT WAS DUE TO POSSIBLE PRESSURIZATION SEALING AT HIGH PWR. GOING THROUGH 80 KIAS; NOISE BECAME INCREASINGLY LOUDER AND SOUNDED LIKE SOMETHING WAS GRINDING. BTWN 80-100 KIAS CAPT INITIATED REJECTED TKOF MANEUVER. MANEUVER WAS PERFORMED PERFECTLY WITH ACFT ON CTRLINE; CALL TO FLT ATTENDANTS TO REMAIN SEATED; AND TWR TO ROLL THE TRUCKS FOR BRAKE INSPECTION. SUBSEQUENTLY; CREW CANCELLED REQUEST FOR EMER VEHICLES AS THERE WERE NO OTHER INDICATIONS OF A PROB; AND THE NOISE SUBSIDED. TAXIED BACK TO THE RAMP; DEPLANED; AND CONTACTED MAINT CTL. EXTERNAL INSPECTION OF THE ACFT PROVIDED NO INDICATIONS OF PROB. JUMPSEATING FLT ATTENDANT SUGGESTED THAT IT SOUNDED LIKE AN AUDIO SYS MALFUNCTION -- WHICH IS WHAT IT ENDED UP BEING. BOARDING MUSIC SYS HAD INADVERTENTLY SWITCHED ON WITH FULL VOLUME AND ALMOST UNBEARABLE 'HISS/SCREECH' IN THE CABIN. MAINT DEFERRED THE SYS AND FLT PROCEEDED WITHOUT FURTHER INCIDENT.

Data retrieved from NASA's ASRS site as of January 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.