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Attributes | |
ACN | 817247 |
Time | |
Date | 200812 |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : zzz.airport |
State Reference | US |
Altitude | agl single value : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | B737-800 |
Operating Under FAR Part | Part 121 |
Flight Phase | ground : takeoff roll |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time last 90 days : 90 flight time total : 5500 flight time type : 500 |
ASRS Report | 817247 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : multi engine pilot : instrument pilot : flight engineer pilot : commercial pilot : atp |
Experience | flight time last 90 days : 80 flight time total : 16000 flight time type : 4800 |
ASRS Report | 817245 |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other flight crewb |
Resolutory Action | flight crew : rejected takeoff |
Consequence | other |
Supplementary | |
Problem Areas | Aircraft |
Primary Problem | Aircraft |
Narrative:
At ZZZ; left engine overheat light illuminated at approximately 60 kts on takeoff roll just after takeoff thrust was achieved. Captain rejected takeoff and light went out. Returned to gate. Maintenance indicated they found a bleed line disconnected and 12-14 insulators on the overheat detection circuit had melted. Maintenance reattached bleed line and replaced the insulators. Attempted another takeoff. Overheat light again illuminated at same point in takeoff roll. Captain rejected takeoff at about 60 kts. Returned to gate and aircraft taken out of service. Callback conversation with reporter revealed the following information: reporter stated that after the first rejected takeoff of the B737-800 and maintenance finding a bleed duct disconnected and 12-14 insulators melted for the overheat detection circuit; he and the captain were quite surprised to see the same overheat light illuminate again; during the second takeoff attempt. Especially since the ground test procedure for the fire/overheat circuit passed; after the repairs had been made. He does not recall if a 'fault' light also illuminated at any of the two times the overheat light illuminated. Reporter stated the bleed duct that maintenance found disconnected after the first rejected takeoff was on the left side of the engine near the compressor case and the overheat circuit was on the upper side approximately in the mid to aft section of the engine. Reporter stated he does not know what the maintenance fix was for the engine overheat light problem after the second rejected tkof.
Original NASA ASRS Text
Title: A B737-800 Captain and First Officer report the left engine overheat light illuminated at approximately 60 knots on two separate takeoff rolls; requiring rejected takeoffs. Maintenance found bleed duct disconnected and 12-14 insulators for the overheat detection circuit melted.
Narrative: At ZZZ; Left Engine Overheat light illuminated at approximately 60 kts on takeoff roll just after takeoff thrust was achieved. Captain rejected takeoff and light went out. Returned to gate. Maintenance indicated they found a bleed line disconnected and 12-14 insulators on the overheat detection circuit had melted. Maintenance reattached bleed line and replaced the insulators. Attempted another takeoff. Overheat light again illuminated at same point in takeoff roll. Captain rejected takeoff at about 60 kts. Returned to gate and aircraft taken out of service. Callback conversation with reporter revealed the following information: Reporter stated that after the first rejected takeoff of the B737-800 and maintenance finding a bleed duct disconnected and 12-14 insulators melted for the overheat detection circuit; he and the Captain were quite surprised to see the same overheat light illuminate again; during the second takeoff attempt. Especially since the ground test procedure for the fire/overheat circuit passed; after the repairs had been made. He does not recall if a 'fault' light also illuminated at any of the two times the overheat light illuminated. Reporter stated the bleed duct that maintenance found disconnected after the first rejected takeoff was on the left side of the engine near the compressor case and the overheat circuit was on the upper side approximately in the mid to aft section of the engine. Reporter stated he does not know what the maintenance fix was for the engine overheat light problem after the second rejected tkof.
Data retrieved from NASA's ASRS site as of May 2009 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.