Narrative:

The flight was routine and uneventful until we were about to turn to intercept the ILS. Just prior to localizer intercept; we got a autopilot fail message on the EICAS. I cancelled the caution and tried to manually control the airplane. I noticed the ailerons could not be moved. After applying considerable input pressure; I regained roll control. During this event we did overshoot our final by a considerable amount. We immediately corrected our course. The first officer scrolled through various mfd synoptic pages and noted no anomalies. Throughout the approach; the roll control felt very heavy and sluggish. With the good VMC weather conditions; we elected to continue the approach. The landing was uneventful. By the time we arrived at the gate; we realized that we could no longer move the control yoke. We contacted maintenance control. A short while later; the mechanic on duty reported the cause to be a water leak that had frozen part of the flight control system.

Google
 

Original NASA ASRS Text

Title: EMB190 Captain experiences frozen aileron controls during LOC intercept. Considerable force is required to overcome the resistance and a successful ILS approach in VMC ensues. Maintenance discovers that leaking water has frozen the aileron controls.

Narrative: The flight was routine and uneventful until we were about to turn to intercept the ILS. Just prior to LOC intercept; we got a Autopilot FAIL message on the EICAS. I cancelled the caution and tried to manually control the airplane. I noticed the ailerons could not be moved. After applying considerable input pressure; I regained roll control. During this event we did overshoot our final by a considerable amount. We immediately corrected our course. The First officer scrolled through various MFD synoptic pages and noted no anomalies. Throughout the approach; the roll control felt very heavy and sluggish. With the good VMC weather conditions; we elected to continue the approach. The landing was uneventful. By the time we arrived at the gate; we realized that we could no longer move the control yoke. We contacted Maintenance Control. A short while later; the mechanic on duty reported the cause to be a water leak that had frozen part of the flight control system.

Data retrieved from NASA's ASRS site as of April 2012 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.