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|
Attributes | |
ACN | 93826 |
Time | |
Date | 198809 |
Day | Tue |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : vny |
State Reference | CA |
Altitude | agl bound lower : 300 agl bound upper : 500 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | general aviation : personal |
Make Model Name | Small Transport |
Flight Phase | cruise other |
Flight Plan | None |
Person 1 | |
Affiliation | Other |
Function | flight crew : single pilot |
Qualification | pilot : instrument pilot : commercial |
Experience | flight time last 90 days : 85 flight time total : 5000 |
ASRS Report | 93826 |
Events | |
Anomaly | aircraft equipment problem : critical other spatial deviation |
Independent Detector | other flight crewa |
Resolutory Action | none taken : unable |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
On a pleasure flight on an evening in 9/88. I experienced an overheating problem with the liquid cooled engine in the small transport. In order to keep the aircraft from losing coolant I had to retard power and was unable to maintain level flight. My altitude became what was less than desired for terrain clearance and I was flying within 300-500' AGL as the engine cooled within its limits. I increased power and slowly worked my way back to van nuys airport for a safe landing. It was found that the radiator had developed a coolant leak and had to be fixed. There was no threat to persons, property or any action that was life threatening. We have developed a better maintenance schedule for our aircraft that was involved.
Original NASA ASRS Text
Title: GA SMT DEVELOPED AN ENGINE COOLENT LEAK AND PLT FLEW AT LOW ALT BACK TO ARPT FOR REPAIR.
Narrative: ON A PLEASURE FLT ON AN EVENING IN 9/88. I EXPERIENCED AN OVERHEATING PROB WITH THE LIQUID COOLED ENG IN THE SMT. IN ORDER TO KEEP THE ACFT FROM LOSING COOLANT I HAD TO RETARD PWR AND WAS UNABLE TO MAINTAIN LEVEL FLT. MY ALT BECAME WHAT WAS LESS THAN DESIRED FOR TERRAIN CLRNC AND I WAS FLYING WITHIN 300-500' AGL AS THE ENG COOLED WITHIN ITS LIMITS. I INCREASED PWR AND SLOWLY WORKED MY WAY BACK TO VAN NUYS ARPT FOR A SAFE LNDG. IT WAS FOUND THAT THE RADIATOR HAD DEVELOPED A COOLANT LEAK AND HAD TO BE FIXED. THERE WAS NO THREAT TO PERSONS, PROPERTY OR ANY ACTION THAT WAS LIFE THREATENING. WE HAVE DEVELOPED A BETTER MAINT SCHEDULE FOR OUR ACFT THAT WAS INVOLVED.
Data retrieved from NASA's ASRS site as of August 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.