37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 108968 |
Time | |
Date | 198904 |
Day | Sat |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : mce |
State Reference | CA |
Altitude | msl bound lower : 1500 msl bound upper : 1500 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : mer |
Operator | other |
Make Model Name | Small Aircraft, Low Wing, 1 Eng, Fixed Gear |
Flight Phase | cruise other cruise other |
Flight Plan | VFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : single pilot |
Qualification | pilot : cfi pilot : commercial pilot : military |
Experience | flight time last 90 days : 45 flight time total : 1500 flight time type : 50 |
ASRS Report | 108968 |
Person 2 | |
Affiliation | government : military |
Function | controller : approach |
Qualification | controller : radar |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : declared emergency none taken : unable |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
While inbound to merced airport and in communication with castle approach I noticed smoke coming out from under instrument panel. Immediately notified castle and squawked XXXX. I reduced power and the smoke disappeared. When I increased the smoke reappeared. I suspected that the smoke was coming from the engine compartment so I made the decision to land immediately at the best possible place--highway 140, west of cunningham rd. I should have turned off all electrical switches, but did not. After a safe landing we investigated the engine compartment and determined the problem to be a malfunctioning voltage regulator. The wires were disconnected and secured and the aircraft was flown to merced airport. The following day, 4/sun/89, the aircraft was ferried to lgb to be repaired.
Original NASA ASRS Text
Title: OFF FIELD LNDG DUE TO SMOKE OF UNKNOWN ORIGIN IN COCKPIT.
Narrative: WHILE INBND TO MERCED ARPT AND IN COM WITH CASTLE APCH I NOTICED SMOKE COMING OUT FROM UNDER INSTRUMENT PANEL. IMMEDIATELY NOTIFIED CASTLE AND SQUAWKED XXXX. I REDUCED PWR AND THE SMOKE DISAPPEARED. WHEN I INCREASED THE SMOKE REAPPEARED. I SUSPECTED THAT THE SMOKE WAS COMING FROM THE ENG COMPARTMENT SO I MADE THE DECISION TO LAND IMMEDIATELY AT THE BEST POSSIBLE PLACE--HWY 140, W OF CUNNINGHAM RD. I SHOULD HAVE TURNED OFF ALL ELECTRICAL SWITCHES, BUT DID NOT. AFTER A SAFE LNDG WE INVESTIGATED THE ENG COMPARTMENT AND DETERMINED THE PROB TO BE A MALFUNCTIONING VOLTAGE REGULATOR. THE WIRES WERE DISCONNECTED AND SECURED AND THE ACFT WAS FLOWN TO MERCED ARPT. THE FOLLOWING DAY, 4/SUN/89, THE ACFT WAS FERRIED TO LGB TO BE REPAIRED.
Data retrieved from NASA's ASRS site as of August 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.