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|
Attributes | |
ACN | 119275 |
Time | |
Date | 198907 |
Day | Fri |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | atc facility : isw |
State Reference | WI |
Altitude | msl bound lower : 8600 msl bound upper : 9000 |
Aircraft 1 | |
Operator | general aviation : personal |
Make Model Name | Small Aircraft, Low Wing, 1 Eng, Retractable Gear |
Flight Phase | cruise other |
Route In Use | enroute airway : zmp |
Flight Plan | IFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : single pilot |
Qualification | pilot : instrument pilot : private |
Experience | flight time last 90 days : 25 flight time total : 650 flight time type : 300 |
ASRS Report | 119275 |
Person 2 | |
Affiliation | government : faa |
Function | controller : radar |
Qualification | controller : radar |
Events | |
Anomaly | aircraft equipment problem : critical altitude deviation : excursion from assigned altitude |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : declared emergency none taken : unable other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
Approximately 45 NM south isw lost altitude (9000 to 8600). Cause was discovery of fuel leak and resultant rapid loss of fuel. Loss of altitude was caused by attention to alternate airports for precautionary landing and calculation of fuel loss and fuel remaining. Cancelled IFR immediately and made rapid VFR descent and landing at isw. Measured 9 gal fuel remaining. Fuel leak caused by completely cracked bracket that held fuel line and vibrated fittings loose. Aircraft had completed a 50 hour inspection prior to this trip. Prevention is a good a&P and FBO that will perform all adequate 50 and 100 hour inspections. The bracket had been cracked for some time so it was missed on both the 100 and 50 hour.
Original NASA ASRS Text
Title: GA SMA ALT DEVIATION EXCURSION FROM CLRNC ALT WHEN PLT WAS DISTRACTED BY A FUEL LEAK.
Narrative: APPROX 45 NM S ISW LOST ALT (9000 TO 8600). CAUSE WAS DISCOVERY OF FUEL LEAK AND RESULTANT RAPID LOSS OF FUEL. LOSS OF ALT WAS CAUSED BY ATTN TO ALTERNATE ARPTS FOR PRECAUTIONARY LNDG AND CALCULATION OF FUEL LOSS AND FUEL REMAINING. CANCELLED IFR IMMEDIATELY AND MADE RAPID VFR DSCNT AND LNDG AT ISW. MEASURED 9 GAL FUEL REMAINING. FUEL LEAK CAUSED BY COMPLETELY CRACKED BRACKET THAT HELD FUEL LINE AND VIBRATED FITTINGS LOOSE. ACFT HAD COMPLETED A 50 HR INSPECTION PRIOR TO THIS TRIP. PREVENTION IS A GOOD A&P AND FBO THAT WILL PERFORM ALL ADEQUATE 50 AND 100 HR INSPECTIONS. THE BRACKET HAD BEEN CRACKED FOR SOME TIME SO IT WAS MISSED ON BOTH THE 100 AND 50 HR.
Data retrieved from NASA's ASRS site as of August 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.