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|
Attributes | |
ACN | 122227 |
Time | |
Date | 198909 |
Day | Mon |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : den |
State Reference | CO |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | IMC |
Light | Dusk |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Large Transport, Low Wing, 3 Turbojet Eng |
Flight Phase | landing other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : cfi pilot : atp pilot : flight engineer |
Experience | flight time last 90 days : 150 flight time total : 15000 flight time type : 4000 |
ASRS Report | 122227 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | inflight encounter : weather other anomaly |
Independent Detector | other flight crewa |
Resolutory Action | none taken : unable |
Consequence | other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
ILS 35R den. WX radar and engine heat used throughout the arrival and approach. Stabilized, coupled approach in smooth conditions with mod rain. Autoplt disconnected at 100', trim and power satisfactory after disconnect. Excessive sink rate detected immediately thereafter. Applied power and pitched up but contacted ground anyway. During the recovery the aircraft bounced twice, landed and rolled out normally. The tailskid was damaged and several interior panels fell down. No injuries were incurred. WX conditions may have contributed to compromising our ability to detect sink rate, but I felt touchdown zone conditions were adequate for a crew of our experience to complete the approach successfully. The sensation experienced was very much like a windshear or wake turbulence and I wonder if traffic ahead or departing the parallel runway might have had an influence.
Original NASA ASRS Text
Title: LGT SUFFERED A HARD LNDG.
Narrative: ILS 35R DEN. WX RADAR AND ENGINE HEAT USED THROUGHOUT THE ARR AND APCH. STABILIZED, COUPLED APCH IN SMOOTH CONDITIONS WITH MOD RAIN. AUTOPLT DISCONNECTED AT 100', TRIM AND POWER SATISFACTORY AFTER DISCONNECT. EXCESSIVE SINK RATE DETECTED IMMEDIATELY THEREAFTER. APPLIED POWER AND PITCHED UP BUT CONTACTED GND ANYWAY. DURING THE RECOVERY THE ACFT BOUNCED TWICE, LANDED AND ROLLED OUT NORMALLY. THE TAILSKID WAS DAMAGED AND SEVERAL INTERIOR PANELS FELL DOWN. NO INJURIES WERE INCURRED. WX CONDITIONS MAY HAVE CONTRIBUTED TO COMPROMISING OUR ABILITY TO DETECT SINK RATE, BUT I FELT TOUCHDOWN ZONE CONDITIONS WERE ADEQUATE FOR A CREW OF OUR EXPERIENCE TO COMPLETE THE APCH SUCCESSFULLY. THE SENSATION EXPERIENCED WAS VERY MUCH LIKE A WINDSHEAR OR WAKE TURBULENCE AND I WONDER IF TFC AHEAD OR DEPARTING THE PARALLEL RWY MIGHT HAVE HAD AN INFLUENCE.
Data retrieved from NASA's ASRS site as of August 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.