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|
Attributes | |
ACN | 127334 |
Time | |
Date | 198910 |
Day | Fri |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : rap |
State Reference | SD |
Altitude | msl bound lower : 29000 msl bound upper : 30000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zmp |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Flight Phase | cruise other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : instrument pilot : commercial pilot : atp |
Experience | flight time last 90 days : 300 flight time total : 9000 flight time type : 400 |
ASRS Report | 127334 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other flight crewa other other : unspecified |
Resolutory Action | flight crew : declared emergency none taken : unable other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
Departed rapid city airport in 10/89. In our climb phase of flight around FL290, we smelled smoke. Shortly after that we saw smoke in the cockpit. We checked with the F/a's to see if they had the same problem in the back. They did. We asked them to check quickly if we had any galley problems or lav problems that they could identify. They said they did not. At that time we declared an emergency and started our return to rapid city airport, since that was the nearest airport. We did the emergency's pertaining to electrical smoke (which we believe we had) and fire, and the other lists that pertained to our situation at that time. We had to wear our O2 masks at this time because of the smoke. We removed all but essential electric from the airplane and operated the rest of the flight with standby power. The smoke stopped during our descent and the air cleared up. The landing was as normal as can be, with us operating with standby electric. After landing we moved onto the taxiway and set the brakes to wait for the emergency equipment to catch up to us and look us over. About this time the F/a called and said the smoke was starting to return into the cabin. At this time we evacuated the airplane. This was done in about 30 seconds with no injuries. We completed all the associated checklists and helped with the evacuate/evacuation. Callback conversation with reporter revealed the following: the problem could not be solved at rap so the aircraft was ferried to a maintenance base. Maintenance found damage to air conditioning pack overheat sensors that allowed excess temperature to be developed, but did not give cockpit warning where the problem was located. The problem happened several days later to the same aircraft so apparent overheat sensing was not the full problem, but the reporter does not know what additional action was taken by maintenance.
Original NASA ASRS Text
Title: FLT CREW OF ACR MLG SMELLED SMOKE AFTER LEVEL OFF. CABIN ATTENDANTS CONFIRMED SMOKE IN THE CABIN, SO EMERGENCY DECLARED RETURN LAND. SMOKE DIMINISHED DURING DESCENT BUT STARTED UP AGAIN AFTERLNDG SO ACFT WAS EVACUATED.
Narrative: DEPARTED RAPID CITY ARPT IN 10/89. IN OUR CLB PHASE OF FLT AROUND FL290, WE SMELLED SMOKE. SHORTLY AFTER THAT WE SAW SMOKE IN THE COCKPIT. WE CHKED WITH THE F/A'S TO SEE IF THEY HAD THE SAME PROB IN THE BACK. THEY DID. WE ASKED THEM TO CHK QUICKLY IF WE HAD ANY GALLEY PROBS OR LAV PROBS THAT THEY COULD IDENT. THEY SAID THEY DID NOT. AT THAT TIME WE DECLARED AN EMER AND STARTED OUR RETURN TO RAPID CITY ARPT, SINCE THAT WAS THE NEAREST ARPT. WE DID THE EMER'S PERTAINING TO ELECTRICAL SMOKE (WHICH WE BELIEVE WE HAD) AND FIRE, AND THE OTHER LISTS THAT PERTAINED TO OUR SITUATION AT THAT TIME. WE HAD TO WEAR OUR O2 MASKS AT THIS TIME BECAUSE OF THE SMOKE. WE REMOVED ALL BUT ESSENTIAL ELECTRIC FROM THE AIRPLANE AND OPERATED THE REST OF THE FLT WITH STANDBY PWR. THE SMOKE STOPPED DURING OUR DSCNT AND THE AIR CLRED UP. THE LNDG WAS AS NORMAL AS CAN BE, WITH US OPERATING WITH STANDBY ELECTRIC. AFTER LNDG WE MOVED ONTO THE TXWY AND SET THE BRAKES TO WAIT FOR THE EMER EQUIP TO CATCH UP TO US AND LOOK US OVER. ABOUT THIS TIME THE F/A CALLED AND SAID THE SMOKE WAS STARTING TO RETURN INTO THE CABIN. AT THIS TIME WE EVACUATED THE AIRPLANE. THIS WAS DONE IN ABOUT 30 SECS WITH NO INJURIES. WE COMPLETED ALL THE ASSOCIATED CHKLISTS AND HELPED WITH THE EVAC. CALLBACK CONVERSATION WITH RPTR REVEALED THE FOLLOWING: THE PROB COULD NOT BE SOLVED AT RAP SO THE ACFT WAS FERRIED TO A MAINT BASE. MAINT FOUND DAMAGE TO AIR CONDITIONING PACK OVERHEAT SENSORS THAT ALLOWED EXCESS TEMPERATURE TO BE DEVELOPED, BUT DID NOT GIVE COCKPIT WARNING WHERE THE PROBLEM WAS LOCATED. THE PROBLEM HAPPENED SEVERAL DAYS LATER TO THE SAME ACFT SO APPARENT OVERHEAT SENSING WAS NOT THE FULL PROB, BUT THE RPTR DOES NOT KNOW WHAT ADDITIONAL ACTION WAS TAKEN BY MAINT.
Data retrieved from NASA's ASRS site as of August 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.