37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 134717 |
Time | |
Date | 199001 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : dca |
State Reference | DC |
Altitude | agl bound lower : 0 agl bound upper : 4000 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tracon : dca |
Operator | common carrier : air taxi |
Make Model Name | Small Transport, Low Wing, 2 Turbojet Eng |
Flight Phase | climbout : takeoff ground : preflight landing other |
Flight Plan | IFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 39 flight time total : 9532 flight time type : 3786 |
ASRS Report | 134717 |
Person 2 | |
Affiliation | Other |
Function | flight crew : first officer |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : far other anomaly other |
Resolutory Action | none taken : anomaly accepted |
Consequence | Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
Landing at dca we had to blow the landing gear down utilizing the emergency air system in an small transport. After disembarking our passenger, maintenance and the director of operations for FBO directed us to fly the aircraft, gear down, from dca-WO0 for corrective maintenance action. This we did. There was no damage to the aircraft either at dca or at WO9. The landing gear problem was corrected by maintenance and the aircraft was flown 2 days later.
Original NASA ASRS Text
Title: SMT LNDG GEAR HAD TO BE BLOWN DOWN PRIOR TO LNDG AT DCA. ACFT WAS FERRIED GEAR DOWN TO WO9.
Narrative: LNDG AT DCA WE HAD TO BLOW THE LNDG GEAR DOWN UTILIZING THE EMER AIR SYS IN AN SMT. AFTER DISEMBARKING OUR PAX, MAINT AND THE DIRECTOR OF OPS FOR FBO DIRECTED US TO FLY THE ACFT, GEAR DOWN, FROM DCA-WO0 FOR CORRECTIVE MAINT ACTION. THIS WE DID. THERE WAS NO DAMAGE TO THE ACFT EITHER AT DCA OR AT WO9. THE LNDG GEAR PROB WAS CORRECTED BY MAINT AND THE ACFT WAS FLOWN 2 DAYS LATER.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.