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|
Attributes | |
ACN | 138911 |
Time | |
Date | 199003 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : fnt |
State Reference | MI |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Light Transport, High Wing, 2 Turboprop Eng |
Flight Phase | climbout : takeoff other other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : instrument pilot : commercial pilot : atp pilot : cfi |
Experience | flight time last 90 days : 240 flight time total : 3400 flight time type : 1800 |
ASRS Report | 138911 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : declared emergency flight crew : rejected takeoff |
Consequence | other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
Our flight originated in flint, mi on 03/thu/90. The first officer and I had completed all the required cockpit checklists and the first flight of day engine checks. After being cleared for takeoff by the tower, we were accelerating down the runway when at approximately 90-90 KTS, the emergency exit hatch (located above the first officer in the cockpit) came off the aircraft. We aborted the takeoff and after telling the tower and our company of the problem, we taxied the aircraft back to the gate (all engine and other indications were normal). Earlier, during the originating checks and again in the pre-taxi checks, the hatch was found to be secure with the handle in the proper position.
Original NASA ASRS Text
Title: ON TKOF ROLL EMERGENCY EXIT HATCH SEPARATED FROM ACFT. TKOF ABORTED.
Narrative: OUR FLT ORIGINATED IN FLINT, MI ON 03/THU/90. THE F/O AND I HAD COMPLETED ALL THE REQUIRED COCKPIT CHECKLISTS AND THE FIRST FLT OF DAY ENGINE CHECKS. AFTER BEING CLRED FOR TKOF BY THE TWR, WE WERE ACCELERATING DOWN THE RWY WHEN AT APPROX 90-90 KTS, THE EMER EXIT HATCH (LOCATED ABOVE THE F/O IN THE COCKPIT) CAME OFF THE ACFT. WE ABORTED THE TKOF AND AFTER TELLING THE TWR AND OUR COMPANY OF THE PROBLEM, WE TAXIED THE ACFT BACK TO THE GATE (ALL ENGINE AND OTHER INDICATIONS WERE NORMAL). EARLIER, DURING THE ORIGINATING CHECKS AND AGAIN IN THE PRE-TAXI CHECKS, THE HATCH WAS FOUND TO BE SECURE WITH THE HANDLE IN THE PROPER POSITION.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.