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|
Attributes | |
ACN | 158437 |
Time | |
Date | 199009 |
Day | Mon |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : stp |
State Reference | MN |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air taxi |
Make Model Name | Small Aircraft |
Flight Phase | landing other |
Flight Plan | None |
Person 1 | |
Affiliation | company : air taxi |
Function | flight crew : single pilot |
Qualification | pilot : commercial pilot : instrument |
Experience | flight time last 90 days : 130 flight time total : 1600 flight time type : 80 |
ASRS Report | 158437 |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other flight crewa |
Resolutory Action | none taken : unable |
Consequence | other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
After conducting a thorough preflight and WX brief I took off from anoka country for st paul airport. All system appeared normal. I monitored ATIS and contacted the checklist, confirming gear down (3 green) with a visibility confirmation in the nacelle mirror. Approach was normal with proper airspeed. There was no indication of problems as I reduced the throttle prior to T/D. I touched the mains first and lowered the nose. The nose gear collapsed (never accepting the aircraft's weight). As the nose dropped, the propellers struck. I went through emergency procedures; shutting down the engines using the mixture and fuel lines. I also shut down the fuel pump and electrical master. After clearing the aircraft from the runway I contacted our director of operations (per operations manual), and met with GADO officers. One week prior to this incident the nose strut actuator was removed, rebuilt and reinstalled. The aircraft had flown once prior to this incident west/O problems. I don't know what more I could have done but I have consulted more experienced airmen.
Original NASA ASRS Text
Title: SMA, ON SECOND FLT ATER LNDG GEAR OVERHAUL, EXPERIENCES NOSE GEAR COLLAPSE ON TOUCHDOWN.
Narrative: AFTER CONDUCTING A THOROUGH PREFLT AND WX BRIEF I TOOK OFF FROM ANOKA COUNTRY FOR ST PAUL ARPT. ALL SYS APPEARED NORMAL. I MONITORED ATIS AND CONTACTED THE CHKLIST, CONFIRMING GEAR DOWN (3 GREEN) WITH A VIS CONFIRMATION IN THE NACELLE MIRROR. APCH WAS NORMAL WITH PROPER AIRSPD. THERE WAS NO INDICATION OF PROBS AS I REDUCED THE THROTTLE PRIOR TO T/D. I TOUCHED THE MAINS FIRST AND LOWERED THE NOSE. THE NOSE GEAR COLLAPSED (NEVER ACCEPTING THE ACFT'S WEIGHT). AS THE NOSE DROPPED, THE PROPS STRUCK. I WENT THROUGH EMER PROCS; SHUTTING DOWN THE ENGS USING THE MIXTURE AND FUEL LINES. I ALSO SHUT DOWN THE FUEL PUMP AND ELECTRICAL MASTER. AFTER CLRING THE ACFT FROM THE RWY I CONTACTED OUR DIRECTOR OF OPS (PER OPS MANUAL), AND MET WITH GADO OFFICERS. ONE WK PRIOR TO THIS INCIDENT THE NOSE STRUT ACTUATOR WAS REMOVED, REBUILT AND REINSTALLED. THE ACFT HAD FLOWN ONCE PRIOR TO THIS INCIDENT W/O PROBS. I DON'T KNOW WHAT MORE I COULD HAVE DONE BUT I HAVE CONSULTED MORE EXPERIENCED AIRMEN.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.