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|
Attributes | |
ACN | 168684 |
Time | |
Date | 199101 |
Day | Fri |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : isb |
State Reference | IA |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | IMC |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tower : isp |
Operator | common carrier : air taxi |
Make Model Name | Small Transport, Low Wing, 2 Turboprop Eng |
Flight Phase | climbout : takeoff other |
Flight Plan | IFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : commercial pilot : instrument |
Experience | flight time last 90 days : 70 flight time total : 10500 flight time type : 100 |
ASRS Report | 168684 |
Person 2 | |
Affiliation | Other |
Function | flight crew : first officer |
Qualification | pilot : cfi pilot : commercial pilot : instrument |
Experience | flight time last 90 days : 70 flight time total : 1108 flight time type : 18 |
ASRS Report | 168683 |
Events | |
Anomaly | aircraft equipment problem : less severe other anomaly other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : regained aircraft control |
Consequence | other Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Situations | |
Airport | other physical facility |
Narrative:
Was taking off at night from sibley, ia. Snowing, snow on runway. Left engine on takeoff failed to come up to full power. Aircraft left the left side of runway. Ground was frozen. Aircraft runway departure corrected with right rudder. Carriage came back onto runway except for main gear. Added power and aircraft came back onto runway. No engine stoppage. I believe as I taxied back down the runway that we had not hit anything. Checked engine power normal, run-up, etc. Nothing abnormal. Takeoff that followed was normal. The aircraft had 2 new engines and the left power lever had been reported binding or dragging when it was test flown after engine installation. I had noticed it on the previous takeoff out of oma, but failed to remember the problem on this initial takeoff. Anyhow, upon landing at oma, it was found that 1 block on the left engine had struck a runway light. Damage was minimal. No vibration, etc.
Original NASA ASRS Text
Title: SNOW FALLING, SNOW ON RWY. ACFT VEERED OFF RWY. CAME BACK ONTO RWY. FLT CREW TAXIED BACK. NEXT TKOF NORMAL. UPON LNDG AT DESTINATION, FOUND STRIKE ON LEFT PROPELLER.
Narrative: WAS TAKING OFF AT NIGHT FROM SIBLEY, IA. SNOWING, SNOW ON RWY. LEFT ENG ON TKOF FAILED TO COME UP TO FULL PWR. ACFT LEFT THE LEFT SIDE OF RWY. GND WAS FROZEN. ACFT RWY DEP CORRECTED WITH RIGHT RUDDER. CARRIAGE CAME BACK ONTO RWY EXCEPT FOR MAIN GEAR. ADDED PWR AND ACFT CAME BACK ONTO RWY. NO ENG STOPPAGE. I BELIEVE AS I TAXIED BACK DOWN THE RWY THAT WE HAD NOT HIT ANYTHING. CHKED ENG PWR NORMAL, RUN-UP, ETC. NOTHING ABNORMAL. TKOF THAT FOLLOWED WAS NORMAL. THE ACFT HAD 2 NEW ENGS AND THE LEFT PWR LEVER HAD BEEN RPTED BINDING OR DRAGGING WHEN IT WAS TEST FLOWN AFTER ENG INSTALLATION. I HAD NOTICED IT ON THE PREVIOUS TKOF OUT OF OMA, BUT FAILED TO REMEMBER THE PROB ON THIS INITIAL TKOF. ANYHOW, UPON LNDG AT OMA, IT WAS FOUND THAT 1 BLOCK ON THE LEFT ENG HAD STRUCK A RWY LIGHT. DAMAGE WAS MINIMAL. NO VIBRATION, ETC.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.