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|
Attributes | |
ACN | 1721664 |
Time | |
Date | 202001 |
Local Time Of Day | 1201-1800 |
Place | |
Locale Reference | ZLA.ARTCC |
State Reference | CA |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Make Model Name | Cessna 150 |
Operating Under FAR Part | Part 91 |
Flight Phase | Cruise |
Route In Use | Direct |
Flight Plan | VFR |
Component | |
Aircraft Component | Engine Air |
Person 1 | |
Function | Single Pilot |
Qualification | Air Traffic Control Fully Certified Flight Crew Commercial Flight Crew Instrument Flight Crew Multiengine |
Experience | Air Traffic Control Non Radar 2 Air Traffic Control Radar 1 Flight Crew Last 90 Days 50 Flight Crew Total 1000 Flight Crew Type 350 |
Events | |
Anomaly | Aircraft Equipment Problem Critical |
Narrative:
I was VFR at 8500 when my aircraft experienced a sudden loss of power. I immediately applied carburetor heat and slightly enriched the mixture; which kept the engine running. Continuously tried a variety of settings with mixture; throttle; and carb heat. When carb heat was removed; the engine seemed to die. After a few minutes and a few hundred feet of descent; I definitively determined this was not carburetor icing and elected to divert to ZZZ airport and [advised ATC]. I suspected some sort of blockage; either to airflow or possible contaminated fuel (though I had sampled the fuel at the last point of departure with negative results). I was able to control the descent and land at ZZZ without incident; where I informed the controller of my safe arrival. A&P on field inspected the aircraft and found the intake air filter was clogged and replaced the filter which solved the problem; aircraft performed satisfactorily on further runup and was returned to service.
Original NASA ASRS Text
Title: C150 pilot reported that a loss of engine power in cruise resulted in a diversion.
Narrative: I was VFR at 8500 when my aircraft experienced a sudden loss of power. I immediately applied carburetor heat and slightly enriched the mixture; which kept the engine running. Continuously tried a variety of settings with mixture; throttle; and carb heat. When carb heat was removed; the engine seemed to die. After a few minutes and a few hundred feet of descent; I definitively determined this was not carburetor icing and elected to divert to ZZZ airport and [advised ATC]. I suspected some sort of blockage; either to airflow or possible contaminated fuel (though I had sampled the fuel at the last point of departure with negative results). I was able to control the descent and land at ZZZ without incident; where I informed the Controller of my safe arrival. A&P on field inspected the aircraft and found the intake air filter was clogged and replaced the filter which solved the problem; aircraft performed satisfactorily on further runup and was returned to service.
Data retrieved from NASA's ASRS site and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.