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|
Attributes | |
ACN | 175941 |
Time | |
Date | 199104 |
Day | Fri |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : ewr |
State Reference | NJ |
Altitude | msl bound lower : 2500 msl bound upper : 2500 |
Environment | |
Flight Conditions | IMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : n90 |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Flight Phase | climbout : takeoff landing other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : commercial pilot : instrument |
Experience | flight time last 90 days : 60 flight time total : 12000 flight time type : 3000 |
ASRS Report | 175941 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other flight crewa |
Resolutory Action | none taken : unable other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
Departed ewr and landing gear would not retract. Performed unable to raise landing gear abnormal procedure as per airline's aircraft flight manual. Landing gear remained down. Aircraft was positioned about 10-15 mi from airport. Advised ATC and returned to ewr. Did not declare an emergency. Aircraft landing was uneventful. Had to stop on runway because of landing gear door dropped down during rollout (as per abnormal procedures). Maintenance found landing gear bypass handle stowed,but not properly. Unable to detect from normal preflight of exterior aircraft. Gasket from handle appeared jammed in seat. First officer preflted and stated handle was flush. Mechanic found handle flush with seat, but further inspection found gasket jammed. Maintenance advised crew that this would be difficult to see on a preflight. Maintenance was advised by maintenance control to replace gasket.
Original NASA ASRS Text
Title: UNABLE TO RAISE GEAR OF MLG AFTER TKOF AND FOLLOWING FLT OPERATIONS PROC INEFFECTIVE. FLT CREW RETURNED AND LANDED EWR.
Narrative: DEPARTED EWR AND LNDG GEAR WOULD NOT RETRACT. PERFORMED UNABLE TO RAISE LNDG GEAR ABNORMAL PROC AS PER AIRLINE'S ACFT FLT MANUAL. LNDG GEAR REMAINED DOWN. ACFT WAS POSITIONED ABOUT 10-15 MI FROM ARPT. ADVISED ATC AND RETURNED TO EWR. DID NOT DECLARE AN EMER. ACFT LNDG WAS UNEVENTFUL. HAD TO STOP ON RWY BECAUSE OF LNDG GEAR DOOR DROPPED DOWN DURING ROLLOUT (AS PER ABNORMAL PROCS). MAINT FOUND LNDG GEAR BYPASS HANDLE STOWED,BUT NOT PROPERLY. UNABLE TO DETECT FROM NORMAL PREFLT OF EXTERIOR ACFT. GASKET FROM HANDLE APPEARED JAMMED IN SEAT. F/O PREFLTED AND STATED HANDLE WAS FLUSH. MECH FOUND HANDLE FLUSH WITH SEAT, BUT FURTHER INSPECTION FOUND GASKET JAMMED. MAINT ADVISED CREW THAT THIS WOULD BE DIFFICULT TO SEE ON A PREFLT. MAINT WAS ADVISED BY MAINT CTL TO REPLACE GASKET.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.