37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 176651 |
Time | |
Date | 199104 |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : atl |
State Reference | GA |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Light Transport, Low Wing, 2 Turboprop Eng |
Flight Phase | ground : preflight |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : instrument |
Experience | flight time last 90 days : 160 flight time total : 7000 flight time type : 2500 |
ASRS Report | 176651 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Events | |
Anomaly | other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | none taken : unable |
Consequence | Other |
Supplementary | |
Primary Problem | Airport |
Air Traffic Incident | other |
Narrative:
After departing tallahassee, fl for atl, we were leveling off at 21000' when the #1 main gen dropped off-line. Emergency procedures were followed and the gen was turned off when it failed to reset. At cruise, a vibration soon developed and the F/a noted sparks out of the #1 engine. The vibration continued to increase so we diverted to macon. A new gen was installed and we continued to atl arriving at aa:30 pm local. Meanwhile, our reduced rest (8 hours) over night in augusta, GA had been cancelled, but our company flight control decided to use us to test fly a test flight. We concluded the test flight and finally dutied out at ab:50 am. We were to go home, rest and duty back in 8 hours to continue our trip. By the time I caught the crew bus, then drove home, it was bb:10 am before actually hitting bed. To make duty in, I had to get up at gg:00 am. Total rest, 4:50. Far's allow airlines to bend crew rest like this continually, as it shows legal on paper. But, as you can see, it's hardly safe. I think it's high time the crew rest requirements are scrutinized before an exhausted crew kills a bunch of people. They'd call it pilot error!
Original NASA ASRS Text
Title: COMPLAINT FROM A COMMUTER LTT CAPT ABOUT COMPANY POLICY REGARDING CREW REST.
Narrative: AFTER DEPARTING TALLAHASSEE, FL FOR ATL, WE WERE LEVELING OFF AT 21000' WHEN THE #1 MAIN GEN DROPPED OFF-LINE. EMER PROCS WERE FOLLOWED AND THE GEN WAS TURNED OFF WHEN IT FAILED TO RESET. AT CRUISE, A VIBRATION SOON DEVELOPED AND THE F/A NOTED SPARKS OUT OF THE #1 ENG. THE VIBRATION CONTINUED TO INCREASE SO WE DIVERTED TO MACON. A NEW GEN WAS INSTALLED AND WE CONTINUED TO ATL ARRIVING AT AA:30 PM LCL. MEANWHILE, OUR REDUCED REST (8 HRS) OVER NIGHT IN AUGUSTA, GA HAD BEEN CANCELLED, BUT OUR COMPANY FLT CTL DECIDED TO USE US TO TEST FLY A TEST FLT. WE CONCLUDED THE TEST FLT AND FINALLY DUTIED OUT AT AB:50 AM. WE WERE TO GO HOME, REST AND DUTY BACK IN 8 HRS TO CONTINUE OUR TRIP. BY THE TIME I CAUGHT THE CREW BUS, THEN DROVE HOME, IT WAS BB:10 AM BEFORE ACTUALLY HITTING BED. TO MAKE DUTY IN, I HAD TO GET UP AT GG:00 AM. TOTAL REST, 4:50. FAR'S ALLOW AIRLINES TO BEND CREW REST LIKE THIS CONTINUALLY, AS IT SHOWS LEGAL ON PAPER. BUT, AS YOU CAN SEE, IT'S HARDLY SAFE. I THINK IT'S HIGH TIME THE CREW REST REQUIREMENTS ARE SCRUTINIZED BEFORE AN EXHAUSTED CREW KILLS A BUNCH OF PEOPLE. THEY'D CALL IT PLT ERROR!
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.