37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 187490 |
Time | |
Date | 199108 |
Day | Wed |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | airport : rld |
State Reference | WA |
Altitude | msl bound lower : 1700 msl bound upper : 1700 |
Environment | |
Flight Conditions | VMC |
Light | Dusk |
Aircraft 1 | |
Controlling Facilities | tower : hou |
Operator | general aviation : personal |
Make Model Name | Small Aircraft |
Flight Phase | cruise other |
Route In Use | approach : visual enroute : direct |
Flight Plan | None |
Person 1 | |
Affiliation | Other |
Function | flight crew : single pilot |
Qualification | pilot : private |
Experience | flight time last 90 days : 10 flight time total : 500 flight time type : 10 |
ASRS Report | 187490 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : declared emergency other |
Consequence | Other Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
Return flight from prosser, wa, to richland, wa, at 1700 ft MSL. About 10 mins into flight engine RPM dropped to approximately 2000 RPM. Cruise RPM was 2450. Engine pitch changed and engine started to run rough. Performed magnetic checks, carburetor heat, mixture, etc checks, nothing worked. At this point it became obvious that I couldn't make airport because I couldn't maintain altitude at 90 mph (normal landing approach speed) and engine conditions were deteriorating. Below was a semi- deserted mobile home park. The 2 northern-most east/west streets were totally unoccupied. I proceeded to make a 360 degree approach to the most northern street and performed a routine landing. Aircraft was undamaged. Subsequent engine examination revealed that #3 piston was gone. Also, the exhaust valve was gone. Probable sequence, supported by visible evidence, indicates that the exhaust valve separated at the valve end and proceeded to destroy the #3 piston and other parts of the engine. There is very little salvageable from this engine. Plane is an experimental and the engine is a converted xyz with approximately 150 hours since overhaul by an FAA certified shop.
Original NASA ASRS Text
Title: ENG FAILURE IN SMA BI-PLANE CREATES THE NEED FOR AN OFF ARPT LNDG.
Narrative: RETURN FLT FROM PROSSER, WA, TO RICHLAND, WA, AT 1700 FT MSL. ABOUT 10 MINS INTO FLT ENG RPM DROPPED TO APPROX 2000 RPM. CRUISE RPM WAS 2450. ENG PITCH CHANGED AND ENG STARTED TO RUN ROUGH. PERFORMED MAG CHKS, CARB HEAT, MIXTURE, ETC CHKS, NOTHING WORKED. AT THIS POINT IT BECAME OBVIOUS THAT I COULDN'T MAKE ARPT BECAUSE I COULDN'T MAINTAIN ALT AT 90 MPH (NORMAL LNDG APCH SPD) AND ENG CONDITIONS WERE DETERIORATING. BELOW WAS A SEMI- DESERTED MOBILE HOME PARK. THE 2 NORTHERN-MOST E/W STREETS WERE TOTALLY UNOCCUPIED. I PROCEEDED TO MAKE A 360 DEG APCH TO THE MOST NORTHERN STREET AND PERFORMED A ROUTINE LNDG. ACFT WAS UNDAMAGED. SUBSEQUENT ENG EXAMINATION REVEALED THAT #3 PISTON WAS GONE. ALSO, THE EXHAUST VALVE WAS GONE. PROBABLE SEQUENCE, SUPPORTED BY VISIBLE EVIDENCE, INDICATES THAT THE EXHAUST VALVE SEPARATED AT THE VALVE END AND PROCEEDED TO DESTROY THE #3 PISTON AND OTHER PARTS OF THE ENG. THERE IS VERY LITTLE SALVAGEABLE FROM THIS ENG. PLANE IS AN EXPERIMENTAL AND THE ENG IS A CONVERTED XYZ WITH APPROX 150 HRS SINCE OVERHAUL BY AN FAA CERTIFIED SHOP.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.