37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 200521 |
Time | |
Date | 199201 |
Day | Tue |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : cae airport : 0a6 |
State Reference | SC |
Altitude | msl bound lower : 14000 msl bound upper : 14000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zjx tracon : cae |
Operator | general aviation : corporate |
Make Model Name | Small Transport, Low Wing, 2 Recip Eng |
Flight Phase | cruise other ground : preflight other |
Flight Plan | IFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : captain oversight : pic |
Qualification | pilot : cfi pilot : instrument pilot : commercial |
Experience | flight time last 90 days : 150 flight time total : 1500 flight time type : 400 |
ASRS Report | 200521 |
Person 2 | |
Affiliation | Other |
Function | flight crew : first officer |
Qualification | pilot : atp pilot : flight engineer |
Experience | flight time last 90 days : 30 flight time total : 4100 flight time type : 50 |
ASRS Report | 200520 |
Events | |
Anomaly | aircraft equipment problem : critical non adherence : published procedure other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | other |
Consequence | Other |
Supplementary | |
Primary Problem | Airport |
Air Traffic Incident | Pilot Deviation other |
Situations | |
Airport | procedure or policy : unspecified |
Narrative:
Approximately 15 mins into flight and level at 14000 ft. We began to get very erratic power surges from the right engine. All engine instruments were indicating normal except for the egt gauge which began to raise rapidly due to the abnormal power surges. Power in the right engine dropped to idle and we began single engine checklist and shutdown procedure and at the same time decided to divert to columbia airport since this was the closest airport. As we were about to shut down right engine we began to get normal power back. As we continued to columbia I flew the airplane and my first officer would handle shut down procedures on engine if necessary. We were then vectored by columbia approach to landing and about 2 mi out on final the right engine quit again as first officer began shut down procedure the power started up again therefore the engine was never feathered. As we began the landing the left engine cut off and we had to be towed into the FBO at airport of landing. I then went to the FAA and filed a report and we contacted 0a6 and advised them not to allow any departures of aircraft that may have been fueled by the same truck we were fueled with. After landing we checked the fuel sumps and found water and sediment in the sample. We had drained all the fuel sumps on the aircraft during preflight. After further inspection by the mechanics in columbia they found approximately 15 - 17 ounces of water in the fuel lines and pumps. I believe the problem arose from receiving contaminated fuel in gastonia, nc, 0a6. I don't believe the fuel truck sumps were drained. Supplemental information from acn 200520. I believe the problem arose at gastonia when we got 60 gals of fuel with water. I do not believe the fuel truck's sumps were drained. Our plane was hangared and the sumps were drained before being fueled.
Original NASA ASRS Text
Title: ENG INFLT SHUTDOWN CREATED BY ACFT FUEL EQUIP PROBLEM.
Narrative: APPROX 15 MINS INTO FLT AND LEVEL AT 14000 FT. WE BEGAN TO GET VERY ERRATIC PWR SURGES FROM THE R ENG. ALL ENG INSTS WERE INDICATING NORMAL EXCEPT FOR THE EGT GAUGE WHICH BEGAN TO RAISE RAPIDLY DUE TO THE ABNORMAL PWR SURGES. PWR IN THE R ENG DROPPED TO IDLE AND WE BEGAN SINGLE ENG CHKLIST AND SHUTDOWN PROC AND AT THE SAME TIME DECIDED TO DIVERT TO COLUMBIA ARPT SINCE THIS WAS THE CLOSEST ARPT. AS WE WERE ABOUT TO SHUT DOWN R ENG WE BEGAN TO GET NORMAL PWR BACK. AS WE CONTINUED TO COLUMBIA I FLEW THE AIRPLANE AND MY FO WOULD HANDLE SHUT DOWN PROCS ON ENG IF NECESSARY. WE WERE THEN VECTORED BY COLUMBIA APCH TO LNDG AND ABOUT 2 MI OUT ON FINAL THE R ENG QUIT AGAIN AS FO BEGAN SHUT DOWN PROC THE PWR STARTED UP AGAIN THEREFORE THE ENG WAS NEVER FEATHERED. AS WE BEGAN THE LNDG THE L ENG CUT OFF AND WE HAD TO BE TOWED INTO THE FBO AT ARPT OF LNDG. I THEN WENT TO THE FAA AND FILED A RPT AND WE CONTACTED 0A6 AND ADVISED THEM NOT TO ALLOW ANY DEPS OF ACFT THAT MAY HAVE BEEN FUELED BY THE SAME TRUCK WE WERE FUELED WITH. AFTER LNDG WE CHKED THE FUEL SUMPS AND FOUND WATER AND SEDIMENT IN THE SAMPLE. WE HAD DRAINED ALL THE FUEL SUMPS ON THE ACFT DURING PREFLT. AFTER FURTHER INSPECTION BY THE MECHS IN COLUMBIA THEY FOUND APPROX 15 - 17 OUNCES OF WATER IN THE FUEL LINES AND PUMPS. I BELIEVE THE PROBLEM AROSE FROM RECEIVING CONTAMINATED FUEL IN GASTONIA, NC, 0A6. I DON'T BELIEVE THE FUEL TRUCK SUMPS WERE DRAINED. SUPPLEMENTAL INFO FROM ACN 200520. I BELIEVE THE PROBLEM AROSE AT GASTONIA WHEN WE GOT 60 GALS OF FUEL WITH WATER. I DO NOT BELIEVE THE FUEL TRUCK'S SUMPS WERE DRAINED. OUR PLANE WAS HANGARED AND THE SUMPS WERE DRAINED BEFORE BEING FUELED.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.