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|
Attributes | |
ACN | 204103 |
Time | |
Date | 199203 |
Day | Sat |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : dtw |
State Reference | MI |
Altitude | msl bound lower : 5000 msl bound upper : 5000 |
Environment | |
Flight Conditions | Mixed |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : dtw tower : dtw |
Operator | common carrier : air carrier |
Make Model Name | Light Transport, Low Wing, 2 Turboprop Eng |
Flight Phase | descent : approach descent other landing other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : flight engineer pilot : commercial pilot : cfi pilot : atp pilot : instrument |
Experience | flight time last 90 days : 20 flight time total : 2600 flight time type : 10 |
ASRS Report | 204103 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer observation : company check pilot |
Qualification | pilot : commercial pilot : instrument pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : overcame equipment problem other |
Consequence | other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
I was receiving initial operating experience as captain on an light transport aircraft from cak to dtw. On climb out from cak we (the crew) noted a split in the power levers and abnormal indications on the right engine (#2). After troubleshooting, we suspected a single redline computer problem and turned that system off. We continued to dtw without further complication until on vectors on a downwind for 21L the right engine would not reduce below 30 percent torque. When the right power lever was moved, the engine would surge +/- 15 percent, causing the aircraft to yaw excessively left and right. We advised dtw tower while on final approach that we would be declaring an emergency due to a precautionary shutdown, and that we would like to go missed approach and secure the engine. We broke off the approach and were vectored back for an approximately 15 mi final again for 21L. The right engine was shut down approximately 5 mi outside the OM. All appropriate checklists were completed and the aircraft was landed without incident. Follow-up with maintenance the next day revealed that the fuel control unit to the engine had failed internally.
Original NASA ASRS Text
Title: LTT ACR ACFT ENG SHUTDOWN AFTER A MALFUNCTION DURING APCH.
Narrative: I WAS RECEIVING INITIAL OPERATING EXPERIENCE AS CAPT ON AN LTT ACFT FROM CAK TO DTW. ON CLBOUT FROM CAK WE (THE CREW) NOTED A SPLIT IN THE PWR LEVERS AND ABNORMAL INDICATIONS ON THE R ENG (#2). AFTER TROUBLESHOOTING, WE SUSPECTED A SINGLE REDLINE COMPUTER PROBLEM AND TURNED THAT SYS OFF. WE CONTINUED TO DTW WITHOUT FURTHER COMPLICATION UNTIL ON VECTORS ON A DOWNWIND FOR 21L THE R ENG WOULD NOT REDUCE BELOW 30 PERCENT TORQUE. WHEN THE R PWR LEVER WAS MOVED, THE ENG WOULD SURGE +/- 15 PERCENT, CAUSING THE ACFT TO YAW EXCESSIVELY L AND R. WE ADVISED DTW TWR WHILE ON FINAL APCH THAT WE WOULD BE DECLARING AN EMER DUE TO A PRECAUTIONARY SHUTDOWN, AND THAT WE WOULD LIKE TO GO MISSED APCH AND SECURE THE ENG. WE BROKE OFF THE APCH AND WERE VECTORED BACK FOR AN APPROX 15 MI FINAL AGAIN FOR 21L. THE R ENG WAS SHUT DOWN APPROX 5 MI OUTSIDE THE OM. ALL APPROPRIATE CHKLISTS WERE COMPLETED AND THE ACFT WAS LANDED WITHOUT INCIDENT. FOLLOW-UP WITH MAINT THE NEXT DAY REVEALED THAT THE FUEL CTL UNIT TO THE ENG HAD FAILED INTERNALLY.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.