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|
Attributes | |
ACN | 207044 |
Time | |
Date | 199204 |
Day | Sun |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : sfo |
State Reference | CA |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | Mixed |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Widebody, Low Wing, 4 Turbojet Eng |
Navigation In Use | Other Other |
Flight Phase | climbout : takeoff |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time last 90 days : 100 flight time total : 10000 flight time type : 100 |
ASRS Report | 207044 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : flight engineer pilot : atp |
Experience | flight time last 90 days : 300 flight time total : 15000 flight time type : 1000 |
ASRS Report | 207409 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : rejected takeoff flight crew : declared emergency |
Consequence | faa : investigated other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
Thrust applied for takeoff (runway 10L sfo). By approximately 50 KTS, aborted takeoff account smoke in cockpit and smoke alarms in lavatories and crew bunk room. While discussing situation with flight attendants over interphone, captain parks aircraft on nearest taxiway off 10L. With reports from flight attendants of increasing cabin smoke, captain elects to evacuate/evacuation aircraft. Evacuate/evacuation proceeded very well and flight attendants did excellent job. Ground support was excellent. No visible damage to aircraft other than smoke saturation.
Original NASA ASRS Text
Title: ACR LARGE WDB ACFT ABORTED TKOF WHEN THE COCKPIT AND CABIN FILLED WITH SMOKE, RESULTING EVAC OF THE ACFT ON THE TAXIWAY.
Narrative: THRUST APPLIED FOR TKOF (RWY 10L SFO). BY APPROX 50 KTS, ABORTED TKOF ACCOUNT SMOKE IN COCKPIT AND SMOKE ALARMS IN LAVATORIES AND CREW BUNK ROOM. WHILE DISCUSSING SITUATION WITH FLT ATTENDANTS OVER INTERPHONE, CAPT PARKS ACFT ON NEAREST TAXIWAY OFF 10L. WITH RPTS FROM FLT ATTENDANTS OF INCREASING CABIN SMOKE, CAPT ELECTS TO EVAC ACFT. EVAC PROCEEDED VERY WELL AND FLT ATTENDANTS DID EXCELLENT JOB. GND SUPPORT WAS EXCELLENT. NO VISIBLE DAMAGE TO ACFT OTHER THAN SMOKE SATURATION.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.