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|
Attributes | |
ACN | 207151 |
Time | |
Date | 199204 |
Day | Sat |
Local Time Of Day | 0001 To 0600 |
Place | |
Locale Reference | airport : sbd |
State Reference | CA |
Altitude | agl bound lower : 0 agl bound upper : 1000 |
Environment | |
Flight Conditions | VMC |
Light | Night |
Aircraft 1 | |
Controlling Facilities | tracon : ont tower : sbd |
Operator | common carrier : air taxi |
Make Model Name | Light Transport, Low Wing, 2 Turbojet Eng |
Flight Phase | climbout : takeoff |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air taxi |
Function | flight crew : first officer |
Qualification | pilot : atp pilot : cfi pilot : commercial pilot : instrument |
Experience | flight time last 90 days : 30 flight time total : 2750 flight time type : 130 |
ASRS Report | 207151 |
Person 2 | |
Affiliation | company : air taxi |
Function | flight crew : captain oversight : pic |
Qualification | pilot : instrument pilot : commercial pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | flight crew : declared emergency other |
Consequence | other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
I was dispatched for a 135 flight. We were to fly from long beach to norton AFB pick up a surgical team and fly to lexington, ky. We departed lgb at XA00 am for norton AFB took on fuel and departed norton. We rotated and the requested 'gear up' but the landing gear unsafe light remained on, we recycled several times with no success. We elected to dump fuel and land at ontario, the landing was normal, but the taxi in to the FBO we noticed a small rubbing noise, after shutdown I got out of the aircraft and found that the pin was left out of the scissors assembly. Due to the fact that it was late, it was dark, the pin was left out prior to departure. The crew has implemented new procedures to avoid the problem happening again.
Original NASA ASRS Text
Title: FLC OF ATX LTT ACFT EXPERIENCED A NOSE GEAR RETRACTION PROBLEM AFTER TKOF.
Narrative: I WAS DISPATCHED FOR A 135 FLT. WE WERE TO FLY FROM LONG BEACH TO NORTON AFB PICK UP A SURGICAL TEAM AND FLY TO LEXINGTON, KY. WE DEPARTED LGB AT XA00 AM FOR NORTON AFB TOOK ON FUEL AND DEPARTED NORTON. WE ROTATED AND THE REQUESTED 'GEAR UP' BUT THE LNDG GEAR UNSAFE LIGHT REMAINED ON, WE RECYCLED SEVERAL TIMES WITH NO SUCCESS. WE ELECTED TO DUMP FUEL AND LAND AT ONTARIO, THE LNDG WAS NORMAL, BUT THE TAXI IN TO THE FBO WE NOTICED A SMALL RUBBING NOISE, AFTER SHUTDOWN I GOT OUT OF THE ACFT AND FOUND THAT THE PIN WAS LEFT OUT OF THE SCISSORS ASSEMBLY. DUE TO THE FACT THAT IT WAS LATE, IT WAS DARK, THE PIN WAS LEFT OUT PRIOR TO DEP. THE CREW HAS IMPLEMENTED NEW PROCS TO AVOID THE PROBLEM HAPPENING AGAIN.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.