37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 211238 |
Time | |
Date | 199205 |
Day | Wed |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | atc facility : gve |
State Reference | FL |
Altitude | msl bound lower : 35000 msl bound upper : 35000 |
Environment | |
Flight Conditions | VMC |
Light | Dusk |
Aircraft 1 | |
Controlling Facilities | artcc : zjx |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Flight Phase | cruise other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time total : 10000 |
ASRS Report | 211238 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | other flight crewa other other : unspecified |
Resolutory Action | flight crew : overcame equipment problem |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | Pilot Deviation other |
Narrative:
Flight was an FAA proving run in an medium large transport, fll to acy. FAA inspector in cockpit jumpseat, another in cabin. Just after level off, cabin inspector gave flight attendant a scenario input card for a loud squeal and air noise around galley door flight attendant called me on interphone just after I had talked to jax center controller. Realized about 15 mins later that my microphone switch on the yoke had stuck open. We (I) had the en route frequency blocked the entire time while we discussed what we would do in that situation (door seal leak, structural damage etc) and then pulled out the MEL and aircraft operating manual to check allowable difference in pilots' altimeters which we had found to be running 130-150 ft at leveloff. (140 allowable listed in operating manual). This was the fifth day of these flts, and we had all observed about 120 ft difference in previous days. As I said, this routine consumed about 15 mins, FAA man on jumpseat, finally remarked that the radio had been very quiet. That was when I realized my transmit switch was stuck, and we had blocked jax center frequency for a considerable time, when they were in fact quite busy.
Original NASA ASRS Text
Title: AN MLG ACR EXPERIENCED A STUCK MIKE, WHILE ON A PROVING RUN, BLOCKING AN ATC FREQ FOR ABOUT 15 MINS.
Narrative: FLT WAS AN FAA PROVING RUN IN AN MLG, FLL TO ACY. FAA INSPECTOR IN COCKPIT JUMPSEAT, ANOTHER IN CABIN. JUST AFTER LEVEL OFF, CABIN INSPECTOR GAVE FLT ATTENDANT A SCENARIO INPUT CARD FOR A LOUD SQUEAL AND AIR NOISE AROUND GALLEY DOOR FLT ATTENDANT CALLED ME ON INTERPHONE JUST AFTER I HAD TALKED TO JAX CTR CTLR. REALIZED ABOUT 15 MINS LATER THAT MY MIKE SWITCH ON THE YOKE HAD STUCK OPEN. WE (I) HAD THE ENRTE FREQ BLOCKED THE ENTIRE TIME WHILE WE DISCUSSED WHAT WE WOULD DO IN THAT SITUATION (DOOR SEAL LEAK, STRUCTURAL DAMAGE ETC) AND THEN PULLED OUT THE MEL AND ACFT OPERATING MANUAL TO CHK ALLOWABLE DIFFERENCE IN PLTS' ALTIMETERS WHICH WE HAD FOUND TO BE RUNNING 130-150 FT AT LEVELOFF. (140 ALLOWABLE LISTED IN OPERATING MANUAL). THIS WAS THE FIFTH DAY OF THESE FLTS, AND WE HAD ALL OBSERVED ABOUT 120 FT DIFFERENCE IN PREVIOUS DAYS. AS I SAID, THIS ROUTINE CONSUMED ABOUT 15 MINS, FAA MAN ON JUMPSEAT, FINALLY REMARKED THAT THE RADIO HAD BEEN VERY QUIET. THAT WAS WHEN I REALIZED MY XMIT SWITCH WAS STUCK, AND WE HAD BLOCKED JAX CTR FREQ FOR A CONSIDERABLE TIME, WHEN THEY WERE IN FACT QUITE BUSY.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.