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|
Attributes | |
ACN | 219172 |
Time | |
Date | 199208 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | atc facility : lee airport : apf |
State Reference | FL |
Altitude | agl bound lower : 0 agl bound upper : 2000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zoa |
Operator | general aviation : instructional |
Make Model Name | Small Aircraft, High Wing, 1 Eng, Fixed Gear |
Flight Phase | descent : approach descent other |
Flight Plan | None |
Person 1 | |
Affiliation | Other |
Function | instruction : instructor |
Qualification | pilot : cfi pilot : atp |
Experience | flight time last 90 days : 260 flight time total : 4000 flight time type : 14 |
ASRS Report | 219172 |
Person 2 | |
Affiliation | Other |
Function | instruction : trainee |
Qualification | pilot : student |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
On aug/thu/92 at approximately XY10 am local time small aircraft X experienced a forced landing in a field south of labelle, fl. There was no visible damage to the aircraft and no injuries to the crew. An emergency was not declared. The flight crew consisting of reporter (instructor pilot) and student pilot were practicing simulated engine failures and ground reference maneuvers over a very large field. At approximately 1800 ft AGL, the instructor pilot applied carburetor heat and ensured the mixture control was full rich prior to retarding the throttle for a simulated engine out approach. During the descent, the engine was occasionally 'cleared' by advancing the throttle to increase engine RPM. An excellent approach (fortunately) to the field was made by the student and flaps full were applied. At approximately 500 ft AGL, a go around was initiated by smoothly advancing the throttle. The engine made a rather muffled popping sound and produced a negligible amount of power. The propeller continued to rotate during the glide until the landing flare where it almost stopped, then rotated again, then finally stopped. At this point the crew applied mixture lean. The airplane suffered no visible damage and the crew uninjured as a result of the forced landing. After inspecting the airplane, engine, and propeller for damage, the master switch was turned on and contact with ft myers approach was initiated. Since turning the master switch on and off to save the battery power was impractical for communication, the crew elected to attempt an engine start. The engine reacted like it was 'flooded' during the restart attempt but, after the third try it started and remained operating for the entire search and rescue to ensure electrical power for communication. At the request of ft myers approach, the ELT was activated for a cumulative 25 mins.
Original NASA ASRS Text
Title: ENG QUIT DURING PRACTICE FORCED LNDG CAUSING AN ACTUAL FORCED LNDG.
Narrative: ON AUG/THU/92 AT APPROX XY10 AM LCL TIME SMA X EXPERIENCED A FORCED LNDG IN A FIELD S OF LABELLE, FL. THERE WAS NO VISIBLE DAMAGE TO THE ACFT AND NO INJURIES TO THE CREW. AN EMER WAS NOT DECLARED. THE FLC CONSISTING OF RPTR (INSTRUCTOR PLT) AND STUDENT PLT WERE PRACTICING SIMULATED ENG FAILURES AND GND REF MANEUVERS OVER A VERY LARGE FIELD. AT APPROX 1800 FT AGL, THE INSTRUCTOR PLT APPLIED CARB HEAT AND ENSURED THE MIXTURE CTL WAS FULL RICH PRIOR TO RETARDING THE THROTTLE FOR A SIMULATED ENG OUT APCH. DURING THE DSCNT, THE ENG WAS OCCASIONALLY 'CLRED' BY ADVANCING THE THROTTLE TO INCREASE ENG RPM. AN EXCELLENT APCH (FORTUNATELY) TO THE FIELD WAS MADE BY THE STUDENT AND FLAPS FULL WERE APPLIED. AT APPROX 500 FT AGL, A GAR WAS INITIATED BY SMOOTHLY ADVANCING THE THROTTLE. THE ENG MADE A RATHER MUFFLED POPPING SOUND AND PRODUCED A NEGLIGIBLE AMOUNT OF PWR. THE PROP CONTINUED TO ROTATE DURING THE GLIDE UNTIL THE LNDG FLARE WHERE IT ALMOST STOPPED, THEN ROTATED AGAIN, THEN FINALLY STOPPED. AT THIS POINT THE CREW APPLIED MIXTURE LEAN. THE AIRPLANE SUFFERED NO VISIBLE DAMAGE AND THE CREW UNINJURED AS A RESULT OF THE FORCED LNDG. AFTER INSPECTING THE AIRPLANE, ENG, AND PROP FOR DAMAGE, THE MASTER SWITCH WAS TURNED ON AND CONTACT WITH FT MYERS APCH WAS INITIATED. SINCE TURNING THE MASTER SWITCH ON AND OFF TO SAVE THE BATTERY PWR WAS IMPRACTICAL FOR COM, THE CREW ELECTED TO ATTEMPT AN ENG START. THE ENG REACTED LIKE IT WAS 'FLOODED' DURING THE RESTART ATTEMPT BUT, AFTER THE THIRD TRY IT STARTED AND REMAINED OPERATING FOR THE ENTIRE SEARCH AND RESCUE TO ENSURE ELECTRICAL PWR FOR COM. AT THE REQUEST OF FT MYERS APCH, THE ELT WAS ACTIVATED FOR A CUMULATIVE 25 MINS.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.