37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 224690 |
Time | |
Date | 199210 |
Day | Thu |
Local Time Of Day | 0601 To 1200 |
Place | |
Locale Reference | airport : lax |
State Reference | CA |
Altitude | agl bound lower : 0 agl bound upper : 5000 |
Environment | |
Flight Conditions | Mixed |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Small Transport, Low Wing, 2 Turboprop Eng |
Flight Phase | climbout : intermediate altitude climbout : takeoff ground : preflight |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time last 90 days : 220 flight time total : 3100 flight time type : 280 |
ASRS Report | 224690 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : less severe |
Independent Detector | other flight crewa other other : unspecified |
Resolutory Action | none taken : unable |
Consequence | other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation other |
Narrative:
After a preflight, I, the first officer, found that the aircraft was ok, while the captain checked the aircraft logs. The captain found the aircraft was out of time and needed an 'a' check. We deplaned the passenger and cancelled the flight so the 'a' check could be accomplished. We did a walkaround and everything seemed normal. We departed from lax-san to cruise at 9000 ft. We took off to the west on runway 25R and on the climb through 5000 ft we heard a thump, we checked all flight and engine instruments and all appeared normal. After landing in san, about a 30 min flight and taxi to the gate, a ground person brought to our attention that the top right outboard engine cowl became loose in-flight and was bent.
Original NASA ASRS Text
Title: AFTER AN 'A' CHK, ENG COWLING COMES LOOSE INFLT AND IS BENT.
Narrative: AFTER A PREFLT, I, THE FO, FOUND THAT THE ACFT WAS OK, WHILE THE CAPT CHKED THE ACFT LOGS. THE CAPT FOUND THE ACFT WAS OUT OF TIME AND NEEDED AN 'A' CHK. WE DEPLANED THE PAX AND CANCELLED THE FLT SO THE 'A' CHK COULD BE ACCOMPLISHED. WE DID A WALKAROUND AND EVERYTHING SEEMED NORMAL. WE DEPARTED FROM LAX-SAN TO CRUISE AT 9000 FT. WE TOOK OFF TO THE W ON RWY 25R AND ON THE CLB THROUGH 5000 FT WE HEARD A THUMP, WE CHKED ALL FLT AND ENG INSTS AND ALL APPEARED NORMAL. AFTER LNDG IN SAN, ABOUT A 30 MIN FLT AND TAXI TO THE GATE, A GND PERSON BROUGHT TO OUR ATTN THAT THE TOP R OUTBOARD ENG COWL BECAME LOOSE INFLT AND WAS BENT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.