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|
Attributes | |
ACN | 230388 |
Time | |
Date | 199212 |
Day | Sun |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | airport : iad |
State Reference | VA |
Altitude | agl bound lower : 0 agl bound upper : 0 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Operator | common carrier : air carrier |
Make Model Name | Light Transport, Low Wing, 2 Turboprop Eng |
Flight Phase | landing other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : cfi pilot : commercial pilot : instrument |
Experience | flight time last 90 days : 100 flight time total : 1400 flight time type : 300 |
ASRS Report | 230388 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | other flight crewa other other : unspecified |
Resolutory Action | none taken : detected after the fact |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
I personally conducted a thorough preflight before we flew the airplane. After a smooth, uneventful touchdown on runway 1L at dulles international airport (iad), the airplane decelerated normally. Upon slowing to approximately 40-50 KTS, the airplane shook violently. We were able to slow down while remaining on the runway centerline. We thought that we had possibly blown a tire, so a gentleman from airport operations drove out to look at our tires after we had turned onto the taxiway. He said that all of our tires appeared to be inflated. While taxiing to the gate, the airplane shook violently again -- very similar to the first time. We called our maintenance operations. The mechanic took a quick look. He said he didn't see anything obviously wrong with the airplane or landing gear. We called our maintenance department again, and they said to see if we could make it home with the airplane. We went out to the airplane and conducted another thorough preflight, and noticed a problem with the right main landing gear. A bolt on the torque knee had come out, and the right landing gear had spun around 180 degrees. Needless to say, the airplane was unable to be flown. The following day, 2 mechanics replaced the landing gear, and we flew back to our base.
Original NASA ASRS Text
Title: AN ACR LTT CREW LOST A BOLT IN THEIR LNDG GEAR CAUSING A VIOLENT SHIMMY.
Narrative: I PERSONALLY CONDUCTED A THOROUGH PREFLT BEFORE WE FLEW THE AIRPLANE. AFTER A SMOOTH, UNEVENTFUL TOUCHDOWN ON RWY 1L AT DULLES INTL ARPT (IAD), THE AIRPLANE DECELERATED NORMALLY. UPON SLOWING TO APPROX 40-50 KTS, THE AIRPLANE SHOOK VIOLENTLY. WE WERE ABLE TO SLOW DOWN WHILE REMAINING ON THE RWY CTRLINE. WE THOUGHT THAT WE HAD POSSIBLY BLOWN A TIRE, SO A GENTLEMAN FROM ARPT OPS DROVE OUT TO LOOK AT OUR TIRES AFTER WE HAD TURNED ONTO THE TXWY. HE SAID THAT ALL OF OUR TIRES APPEARED TO BE INFLATED. WHILE TAXIING TO THE GATE, THE AIRPLANE SHOOK VIOLENTLY AGAIN -- VERY SIMILAR TO THE FIRST TIME. WE CALLED OUR MAINT OPS. THE MECH TOOK A QUICK LOOK. HE SAID HE DIDN'T SEE ANYTHING OBVIOUSLY WRONG WITH THE AIRPLANE OR LNDG GEAR. WE CALLED OUR MAINT DEPT AGAIN, AND THEY SAID TO SEE IF WE COULD MAKE IT HOME WITH THE AIRPLANE. WE WENT OUT TO THE AIRPLANE AND CONDUCTED ANOTHER THOROUGH PREFLT, AND NOTICED A PROB WITH THE R MAIN LNDG GEAR. A BOLT ON THE TORQUE KNEE HAD COME OUT, AND THE R LNDG GEAR HAD SPUN AROUND 180 DEGS. NEEDLESS TO SAY, THE AIRPLANE WAS UNABLE TO BE FLOWN. THE FOLLOWING DAY, 2 MECHS REPLACED THE LNDG GEAR, AND WE FLEW BACK TO OUR BASE.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.