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|
Attributes | |
ACN | 233975 |
Time | |
Date | 199302 |
Day | Mon |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : lga airport : jfk |
State Reference | NY |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : n90 |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Navigation In Use | Other Other |
Flight Phase | descent : approach descent other landing other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : atp |
Experience | flight time last 90 days : 200 flight time total : 23000 flight time type : 19000 |
ASRS Report | 233975 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp pilot : flight engineer |
Experience | flight time last 90 days : 180 flight time total : 15600 flight time type : 3000 |
ASRS Report | 233987 |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
During descent into lga we heard a loud bang in the cockpit. After evaluation we determined that the right engine was not developing normal thrust. The captain exercised his emergency authority and diverted to jfk for longer runway. We operated the engine at idle thrust until landing roll and then shut down normally. Maintenance inspection revealed last turbine stage failure and stator damage. The decision to keep the engine running was based on the fact that the only abnormal engine parameters were slightly lower EPR and N-1. The other indications were normal, fuel flow, oil pressure, egt and N-2. Also, the airport was only 8-10 mi away.
Original NASA ASRS Text
Title: AN MLG ACR CREW HAD AN INTERNAL FAILURE OF AN ENG.
Narrative: DURING DSCNT INTO LGA WE HEARD A LOUD BANG IN THE COCKPIT. AFTER EVALUATION WE DETERMINED THAT THE R ENG WAS NOT DEVELOPING NORMAL THRUST. THE CAPT EXERCISED HIS EMER AUTHORITY AND DIVERTED TO JFK FOR LONGER RWY. WE OPERATED THE ENG AT IDLE THRUST UNTIL LNDG ROLL AND THEN SHUT DOWN NORMALLY. MAINT INSPECTION REVEALED LAST TURBINE STAGE FAILURE AND STATOR DAMAGE. THE DECISION TO KEEP THE ENG RUNNING WAS BASED ON THE FACT THAT THE ONLY ABNORMAL ENG PARAMETERS WERE SLIGHTLY LOWER EPR AND N-1. THE OTHER INDICATIONS WERE NORMAL, FUEL FLOW, OIL PRESSURE, EGT AND N-2. ALSO, THE ARPT WAS ONLY 8-10 MI AWAY.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.