37000 Feet | Browse and search NASA's Aviation Safety Reporting System |
|
Attributes | |
ACN | 244672 |
Time | |
Date | 199306 |
Day | Thu |
Place | |
Locale Reference | atc facility : mke |
State Reference | WI |
Altitude | msl bound lower : 12000 msl bound upper : 28000 |
Environment | |
Flight Conditions | VMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zmp |
Operator | common carrier : air carrier |
Make Model Name | Medium Large Transport, Low Wing, 2 Turbojet Eng |
Flight Phase | cruise other descent other other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : flight engineer pilot : atp |
Experience | flight time last 90 days : 185 flight time total : 10500 flight time type : 2400 |
ASRS Report | 244672 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : instrument pilot : commercial |
Events | |
Anomaly | aircraft equipment problem : critical |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | aircraft : equipment problem dissipated flight crew : declared emergency flight crew : overcame equipment problem flight crew : exited adverse environment |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Narrative:
At FL280, cabin pressure was climbing at 1000 FPM. Declared an emergency and initiated descent as cabin reached 10000 ft. Accomplished appropriate checklist. Regained control of cabin at 12000 ft. System worked normally for remainder of flight to msp. Suspect icing up of outflow valve due to icing conditions we were in the last 45 mins before the pressurization problem.
Original NASA ASRS Text
Title: EMER DECLARED WITH ASSOCIATED DSCNT WHEN LOSS OF CABIN PRESSURE EXPERIENCED BY ACR MLG.
Narrative: AT FL280, CABIN PRESSURE WAS CLBING AT 1000 FPM. DECLARED AN EMER AND INITIATED DSCNT AS CABIN REACHED 10000 FT. ACCOMPLISHED APPROPRIATE CHKLIST. REGAINED CTL OF CABIN AT 12000 FT. SYS WORKED NORMALLY FOR REMAINDER OF FLT TO MSP. SUSPECT ICING UP OF OUTFLOW VALVE DUE TO ICING CONDITIONS WE WERE IN THE LAST 45 MINS BEFORE THE PRESSURIZATION PROB.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.