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|
Attributes | |
ACN | 246928 |
Time | |
Date | 199307 |
Day | Thu |
Local Time Of Day | 1201 To 1800 |
Place | |
Locale Reference | atc facility : pxv |
State Reference | IN |
Altitude | msl bound lower : 25000 msl bound upper : 39000 |
Environment | |
Flight Conditions | IMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | artcc : zid tower : fra |
Operator | general aviation : corporate |
Make Model Name | Light Transport, Low Wing, 2 Turbojet Eng |
Flight Phase | cruise other descent other other |
Route In Use | enroute : direct |
Flight Plan | IFR |
Person 1 | |
Affiliation | Other |
Function | flight crew : captain oversight : pic |
Qualification | pilot : atp |
Experience | flight time last 90 days : 140 flight time total : 6700 flight time type : 2400 |
ASRS Report | 246928 |
Person 2 | |
Affiliation | Other |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : critical altitude deviation : excursion from assigned altitude inflight encounter : weather non adherence : published procedure non adherence : clearance other anomaly other |
Independent Detector | other flight crewa |
Resolutory Action | flight crew : overcame equipment problem other |
Consequence | Other |
Supplementary | |
Primary Problem | Flight Crew Human Performance |
Air Traffic Incident | Pilot Deviation |
Narrative:
While on a flight from cvg to wld at FL390, we noticed a broken line of convective WX on radar near the pxv VOR. We took a course that would take us between 2 cells that were 20 mi apart. When we were abeam pxv VOR we encountered moderate turbulence and some wind shear that caused our airspeed to increase and then decrease, so we decreased the power to maintain our speed of .76 mach. After a min or so, I increased power back to normal cruise. At that point the right engine flamed out. We had to descend to FL250 for a relight at that point. We advised ATC as soon as possible of our situation and our intentions. The purpose for this flight was to repos to wld to have loaner engines removed and new engines installed. I believe the major cause of this event was a problem in the loaner engine, but also the use of air ignition might have prevented the flameout even with the engine problem.
Original NASA ASRS Text
Title: ALTDEV ALT EXCURSION TO RELIGHT 1 FLAMED OUT ENG. INFLT ENG SHUTDOWN.
Narrative: WHILE ON A FLT FROM CVG TO WLD AT FL390, WE NOTICED A BROKEN LINE OF CONVECTIVE WX ON RADAR NEAR THE PXV VOR. WE TOOK A COURSE THAT WOULD TAKE US BTWN 2 CELLS THAT WERE 20 MI APART. WHEN WE WERE ABEAM PXV VOR WE ENCOUNTERED MODERATE TURB AND SOME WIND SHEAR THAT CAUSED OUR AIRSPD TO INCREASE AND THEN DECREASE, SO WE DECREASED THE PWR TO MAINTAIN OUR SPD OF .76 MACH. AFTER A MIN OR SO, I INCREASED PWR BACK TO NORMAL CRUISE. AT THAT POINT THE R ENG FLAMED OUT. WE HAD TO DSND TO FL250 FOR A RELIGHT AT THAT POINT. WE ADVISED ATC ASAP OF OUR SIT AND OUR INTENTIONS. THE PURPOSE FOR THIS FLT WAS TO REPOS TO WLD TO HAVE LOANER ENGS REMOVED AND NEW ENGS INSTALLED. I BELIEVE THE MAJOR CAUSE OF THIS EVENT WAS A PROB IN THE LOANER ENG, BUT ALSO THE USE OF AIR IGNITION MIGHT HAVE PREVENTED THE FLAMEOUT EVEN WITH THE ENG PROB.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.