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|
Attributes | |
ACN | 251793 |
Time | |
Date | 199309 |
Day | Thu |
Local Time Of Day | 1801 To 2400 |
Place | |
Locale Reference | atc facility : hya airport : bos |
State Reference | MA |
Altitude | msl bound lower : 6000 msl bound upper : 6000 |
Environment | |
Flight Conditions | IMC |
Light | Daylight |
Aircraft 1 | |
Controlling Facilities | tracon : hya |
Operator | common carrier : air carrier |
Make Model Name | Small Transport |
Flight Phase | cruise other other |
Flight Plan | IFR |
Person 1 | |
Affiliation | company : air carrier |
Function | flight crew : captain oversight : pic |
Qualification | pilot : cfi pilot : commercial pilot : atp pilot : instrument |
Experience | flight time last 90 days : 150 flight time total : 10700 flight time type : 7000 |
ASRS Report | 251793 |
Person 2 | |
Affiliation | company : air carrier |
Function | flight crew : first officer |
Qualification | pilot : commercial pilot : instrument |
Events | |
Anomaly | aircraft equipment problem : critical other anomaly other |
Independent Detector | aircraft equipment other aircraft equipment : unspecified other flight crewa |
Resolutory Action | controller : issued new clearance flight crew : overcame equipment problem other |
Consequence | Other |
Supplementary | |
Primary Problem | Aircraft |
Air Traffic Incident | other |
Narrative:
We experienced flagging off of all navigation and electrical flight instruments for about 5 seconds as we got a master caution light illumination as well as a #1 inverter failed light. Per the pilot's operating handbook, we selected the defective inverter off and, as a crew, discussed our situation and decided to return to boston's 15 scattered, 40 broken, 15 mi visibility WX which was much preferable to hyannis' 1000 ft overcast, 6 mi visibility and haze. The cold front in the northeast area made good sense for us to head north as the further north we could go, the more VFR the WX. We advised ATC of our electrical malfunction, but requested no further assistance at the time. We landed bos without further problems and were surprised the emergency vehicles were awaiting by the side of the runway. Once again, we stated no assistance was needed and we taxied to the ramp where maintenance repaired our beleagured craft.
Original NASA ASRS Text
Title: AN ACR SMT DIVERTED TO ITS ALTERNATE WITH AN INST AND ELECTRICAL FAILURE.
Narrative: WE EXPERIENCED FLAGGING OFF OF ALL NAV AND ELECTRICAL FLT INSTS FOR ABOUT 5 SECONDS AS WE GOT A MASTER CAUTION LIGHT ILLUMINATION AS WELL AS A #1 INVERTER FAILED LIGHT. PER THE PLT'S OPERATING HANDBOOK, WE SELECTED THE DEFECTIVE INVERTER OFF AND, AS A CREW, DISCUSSED OUR SIT AND DECIDED TO RETURN TO BOSTON'S 15 SCATTERED, 40 BROKEN, 15 MI VISIBILITY WX WHICH WAS MUCH PREFERABLE TO HYANNIS' 1000 FT OVCST, 6 MI VISIBILITY AND HAZE. THE COLD FRONT IN THE NE AREA MADE GOOD SENSE FOR US TO HEAD N AS THE FURTHER N WE COULD GO, THE MORE VFR THE WX. WE ADVISED ATC OF OUR ELECTRICAL MALFUNCTION, BUT REQUESTED NO FURTHER ASSISTANCE AT THE TIME. WE LANDED BOS WITHOUT FURTHER PROBS AND WERE SURPRISED THE EMER VEHICLES WERE AWAITING BY THE SIDE OF THE RWY. ONCE AGAIN, WE STATED NO ASSISTANCE WAS NEEDED AND WE TAXIED TO THE RAMP WHERE MAINT REPAIRED OUR BELEAGURED CRAFT.
Data retrieved from NASA's ASRS site as of July 2007 and automatically converted to unabbreviated mixed upper/lowercase text. This report is for informational purposes with no guarantee of accuracy. See NASA's ASRS site for official report.